Accident Lockheed L-188A Electra N5533,
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ASN Wikibase Occurrence # 333705
 
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Date:Tuesday 4 October 1960
Time:17:40
Type:Silhouette image of generic L188 model; specific model in this crash may look slightly different    
Lockheed L-188A Electra
Owner/operator:Eastern Air Lines
Registration: N5533
MSN: 1062
Year of manufacture:1959
Total airframe hrs:3526 hours
Engine model:Allison 501-D13
Fatalities:Fatalities: 62 / Occupants: 72
Aircraft damage: Destroyed, written off
Category:Accident
Location:ca 1 km E off Boston-Logan International Airport, MA (BOS) -   United States of America
Phase: Initial climb
Nature:Passenger - Scheduled
Departure airport:Boston-Logan International Airport, MA (BOS/KBOS)
Destination airport:Philadelphia International Airport, PA (PHL/KPHL)
Investigating agency: CAB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
An Eastern Air Lines Lockheed L-188A Electra, N5533, crashed into Winthrop Bay immediately following takeoff from runway 9 at Boston-Logan International Airport, Massachusetts.
Eastern Air Lines flight 375 was a domestic flight from Boston to Atlanta, Georgia with en route stops at Philadelphia, Pennsylvania; Charlotte, North Carolina; and Greenville, South Carolina. The flight taxied to runway 9 where takeoff was commenced at approximately 17:39. A few seconds after taking off from runway 05, the Electra struck a flock of starlings. A number of these birds were ingested in engine no.1, 2 and 4.
The engine number 1 propeller was feathered by an autofeather system, as designed. Engine number 2 and 4 experienced substantial losses of power, but, by design, those propellers were prevented by the airplane’s system from also feathering automatically, since only one propeller is permitted to autofeather when the autofeather system is armed. The abrupt and intermittent loss and recovery of power and associated thrust asymmetry caused the airplane to yaw to the left and decelerate below the speed at which directional control could be maintained. The left wing dropped, the nose pitched up, and the airplane rolled left and fell almost vertically into Winthrop Bay near the end of the runway.

Following the crash, the investigators recovered approximately 75 starling carcasses on/near the presumed area on the runway where the bird encounter occurred.

PROBABLE CAUSE: "The unique and critical sequence of the loss and recovery of engine power following bird ingestion, resulting in loss of airspeed and control during takeoff. "

Accident investigation:
cover
  
Investigating agency: CAB
Report number: final report
Status: Investigation completed
Duration: 1 year and 10 months
Download report: Final report

Sources:


Location

Images:


photo (c) Civil Aeronautics Board (CAB); Boston-Logan International Airport, MA (BOS); October 1960; (publicdomain)


photo (c) Civil Aeronautics Board (CAB); Boston-Logan International Airport, MA (BOS); October 1960; (publicdomain)


photo (c) Civil Aeronautics Board (CAB); Boston-Logan International Airport, MA (BOS); October 1960; (publicdomain)


photo (c) CAB; near Boston-Logan International Airport, MA (BOS); 04 October 1960; (publicdomain)

Revision history:

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