Accident
Last updated: 19 June 2013
| Estado: | Final |
| Fecha: | 06 MAY 1981 |
| Hora: | 10:50 |
| Tipo: | Boeing EC-135N |
| Operador: | United States Air Force - USAF |
| Registración: | 61-0328 |
| Numéro de série: | 18235/C13 |
| Año de Construcción: | 1961-11-14 (19 years 6 months) |
| Horas Totales de la Célula: | 13471 |
| Motores: | 4 Pratt & Whitney TF33-PW-102 |
| Tripulación: | Fatalidades: 17 / Ocupantes: 17 |
| Pasajeros: | Fatalidades: 4 / Ocupantes: 4 |
| Total: | Fatalidades: 21 / Ocupantes: 21 |
| Daños en la Aeronave: | Anulado |
| Consecuencias: | Written off (damaged beyond repair) |
| Ubicación: | 3 km (1.9 milles) NNE of Walkersville, MD (Estados Unidos de América)
 |
| Fase: | En ruta (ENR) |
| Naturaleza: | Entrenamiento Militar |
| Aeropuerto de Salida: | Dayton-Wright Patterson AFB, OH (FFO/KFFO), Estados Unidos de América |
| Aeropuerto de Llegada: | Dayton-Wright Patterson AFB, OH (FFO/KFFO), Estados Unidos de América |
Descripción:EC-135N aircraft 61-0328, call sign AGAR 23, was scheduled for an Advanced Range Instrumented Aircraft (ARIA) training mission out of Wright-Patterson AFB. The mission was designed provide training for the navigator and primar mission electronic equipment (PMEE) operators. On board the aircraft were 17 crewmembers and four authorized passengers. AGAR 23 departed at 10:05 and climbed to FL290, which was reached at 10:30. The aircraft commander occupied the right pilot seat and a passenger, his wife, occupied the left pilot seat.
For undetermined reasons, the aircraft pitch trim moved to the full nose-down position. The autopilot can overcome the trim until near full nose-down. The aircraft then rapidly pitched over, most likely upon release of the autopilot, and induced sufficient negative g forces to cause the generators to trip off line and loss of all AC electrical power. The pitch trim could not then be moved electrically. This condition, while unusual, can be easily controlled if prompt corrective action is taken; however, if corrective action is delayed approximately 8 sec., the aircraft pitch angle will be greater than 30 deg. nose-down and the airspeed in excess of 350 KIAS. Under these conditions,the aircraft cannot be controlled until the pitch trim is moved toward neutral. While it is clear that recovery was delayed, the reason for the delay is unknown. The aircraft became uncontrollable and entered a steep descent. The aircraft emerged from the clouds at 2,000 ft. AGL. Airspeed was in excess of 400 KTAS and dive angle was 20 to 30 deg. Engine power was above 2.0 EPR. At approximately 1,500 ft. MSL an explosion occurred inside the pressurized compartment of the fuselage and weakened the aircraft structure to the extent that catastrophic failure of the aircraft followed immediately.
Fuentes:
Sample newspaper article from Newspaperarchive.com
Fotos
Map
This map shows the airport of departure and the intended destination of the flight. The line between the airports does
not display the exact flight path.
Distance from Dayton-Wright Patterson AFB, OH to Dayton-Wright Patterson AFB, OH as the crow flies is 0 km (0 miles).
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Boeing C-135
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