Accident Boeing 747-251B N637US,
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ASN Wikibase Occurrence # 325031
 

Date:Tuesday 1 March 1994
Time:13:38
Type:Silhouette image of generic B742 model; specific model in this crash may look slightly different    
Boeing 747-251B
Owner/operator:Northwest Airlines
Registration: N637US
MSN: 23548/644
Year of manufacture:1986
Total airframe hrs:31798 hours
Engine model:Pratt & Whitney JT9D-7R4G2
Fatalities:Fatalities: 0 / Occupants: 245
Aircraft damage: Substantial, repaired
Category:Accident
Location:Tokyo-Narita Airport (NRT) -   Japan
Phase: Landing
Nature:Passenger - Scheduled
Departure airport:Hong Kong-Kai Tak International Airport (HKG/VHHH)
Destination airport:Tokyo-Narita Airport (NRT/RJAA)
Investigating agency: ARAIC
Confidence Rating: Accident investigation report completed and information captured
Narrative:
Northwest Airlines Flight 18 had departed from Hong Kong for a flight to New York-JFK with an intermediate stop at Tokyo-Narita, Japan. The flight, touchdown, and initial landing rollout at Narita, were routine. Engine thrust reversing was normal on all four engines until the flight crew moved the engine power levers out of reverse thrust at about 90 knots. During the rollout, the No. 1 engine and pylon rotated downward about the midspar pylon-to-wing fittings into a position in which the lower forward part of the engine nose cowl contacted the runway. The airplane was subsequently stopped on a taxiway, with the front of the No. 1 engine still contacting the ground. The lower forward engine nose cowl had been ground away as it slid along the runway. A fire near the No. 1 engine was rapidly extinguished by local fire fighters, and all passengers remained aboard. They were subsequently deplaned via portable boarding stairs about 30 minutes after the airplane was brought to a stop. There were no injuries.
Maintenance and inspection personnel who worked on the airplane were not adequately trained and qualified to perform the required maintenance and inspection functions. In addition, the work environment for the heavy maintenance of the airplane was inadequate and contributed to an effort producing situation for the workers.

PROBABLE CAUSE: "When C check of the aircraft was conducted, the retainer for the diagonal brace aft fuse pin of No.1 nacelle strut was removed and the aircraft was returned to service without reinstalling the retainer. In the course of the flights after this, the fuse pin moved, disconnecting the diagonal brace at the aft joint.
It is estimated that when the thrust reverser was deployed during the landing roll under such circumstances, the forward fuse pin of the upper link was fractured due to a load in excess of the design rupture strength, dangling the forward portion of No.1 engine and a fire on leaked oil and fuel broke out in the aft portion of the nacelle strut."

Accident investigation:
cover
  
Investigating agency: ARAIC
Report number: 
Status: Investigation completed
Duration: 2 years and 9 months
Download report: Final report

Sources:

NTSB/SIR-94/02

Location

Images:


photo (c) NTSB; Tokyo-Narita Airport (NRT/RJAA); 01 March 1994; (publicdomain)


photo (c) JTSB; Tokyo-Narita Airport (NRT/RJAA); 01 March 1994


photo (c) JTSB; Tokyo-Narita Airport (NRT/RJAA); 01 March 1994


photo (c) JTSB; Tokyo-Narita Airport (NRT/RJAA); 01 March 1994

Revision history:

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