Status: | Accident investigation report completed and information captured |
Datum: | Freitag 23 September 1994 |
Zeit: | 19:15 |
Flugzeugtyp: |  Lockheed L-100-30 Hercules |
Betrieben durch: | Heavylift Cargo Airlines |
Gemietet von : | Pelita Air Service |
Kennzeichen: | PK-PLV |
Werknummer: | 4826 |
Baujahr: | 1979 |
Betriebsstunden: | 15223 |
Triebwerk: | 4 Allison 501-D22A |
Besatzung: | Todesopfer: 3 / Insassen: 6 |
Fluggäste: | Todesopfer: 3 / Insassen: 6 |
Gesamt: | Todesopfer: 6 / Insassen: 12 |
Sachschaden: | Zerstört |
Konsequenzen: | Written off (damaged beyond repair) |
Unfallort: | 0,5 km (0.3 Meilen) S vom Land entfernt von Hong Kong-Kai Tak International Airport (HKG) ( Hong Kong)
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Flugphase: | Start (TOF) |
Betriebsart: | Leerflug |
Flug von: | Hong Kong-Kai Tak International Airport (HKG/VHHH), |
Flug nach: | Jakarta-Halim Perdana Kusuma Airport (HLP/WIHH), Indonesien |
Unfallbericht:Hercules aircraft PK-PLV and the operating and positioning crews were deployed from their home base in Jakarta, Indonesia, to Hong Kong on 21 September 1994 to carry out a contract for Heavy Lift Cargo Airlines. The contract involved making one return trip from Hong Kong to Hanoi on 22 September and another on 23 September to transport Vietnamese illegal immigrants in Hong Kong back to Vietnam. The crew involved in the accident flight had operated the return trip on 22 September and had rested on 23 September while the other crew operated the flight to Hanoi earlier that day. When PK-PLV arrived back in Hong Kong at 17:35 hrs on 23 September 1994, the operating crew were relieved by the rested crew for the flight back to Jakarta. The captain who took over was verbally informed by his predecessor that there were no problems with the aircraft. The ground mechanic fully checked the aircraft and had it refuelled to give a total of 45,000 lb fuel on board.
With both crews back on board, the captain started the engines at 18:31 hrs. The start was normal and at 18:49 hrs he used reverse thrust to back out from Bay 78 to position on the taxiway. The captain then taxied to the holding point at A1, for a takeoff on runway 13. The time taken to reach the holding point was approximately 18 minutes. This was partly due to the pilot's unfamiliarity with the taxy route and partly to a delay of some six minutes to give way to another aircraft. During the ground movement, the captain completed the normal taxy and before takeoff checks. He also gave a takeoff briefing to his crew. After a delay of 2,5 minutes at the holding point, he was cleared by Air Traffic Control (ATC) to line up on the runway behind landing traffic and wait.
PK-PLV was subsequently cleared for takeoff at 19:14 hrs, two minutes after the traffic had landed. At that time it was already dark with a visibility of 9 Km. There was light rain and the runway was wet. The surface wind was 090°/12 kt. The captain in the left seat was the handling pilot and both the first officer and Flight Engineer occupied their normal seats. Also in the cockpit were four other personnel. The captain of the positioning crew was in the observer's seat and the positioning first officer, another positioning crew member and the Senior Purser/Air Loadmaster were seated on the bunk at the rear of the cockpit. The other five personnel occupied seats in the passenger compartment.
After the aircraft lined up on the runway the captain held the aircraft on the wheel brakes while setting 5,000 in-lb of torque on all 4 engines. As this power figure was achieved he made a check of the engine instruments before releasing the brakes and applying full power. To the occupants of the aircraft the takeoff seemed normal, although two external observers commented that the acceleration seemed slightly slow for a Hercules. When the first officer called "70 kt", the captain moved his left hand from the steering tiller to the control column. The first officer made the normal takeoff calls of " V1", "VR" and "V2" The captain rotated the aircraft at VR and, after the first officer had announced "positive rate", he called for "gear up". He saw the first officer reach for, and move the gear lever. Then he heard "a high pitched noise" from his right and found that he was applying left aileron because the aircraft was banking right. Looking at the engine instruments, he noted that No. 4 RPM was indicating higher than normal and that No. 4 Turbine Inlet Temperature (TIT) was reducing slowly. The captain recalled his airspeed at that time to be about 122 or 123 kt and he was by then applying left rudder and full left aileron. The aircraft kept turning right and started buffeting. The captain tried bringing No. 1 throttle back a little to stop the turn but this action had no apparent effect. He then called "Take action for No. 4", but there was no confirmation that any remedial action was attempted by any of the other flight crew members.
As the aircraft continued on its right turn at very low altitude its right main gear briefly contacted the grass strip adjacent to the runway. It finally impacted the water 500 metres off-shore in Kowloon Bay on a southerly heading, with some right bank and in a nose low attitude. As the aircraft gradually submerged, 2 life rafts came to the surface and were utilised by the 7 occupants who had managed to escape. Of these 7 survivors 1 died before arrival at hospital. The remaining 5 occupants were later found drowned.
Probable Cause:
CAUSAL FACTORS:
1. The No. 4 propeller entered the Beta range shortly after the aircraft became airborne.
2. The crew were unable to retain control of the aircraft following this occurrence.
Accident investigation:
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Investigating agency: | CAD Hong Kong  |
Status: | Investigation completed |
Duration: | 2 years | Accident number: | AAR 3-96 | Download report: | Final report
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Informationsquelle:
» ICAO Adrep Summary 5/94 (#64)
» Scramble 185
Sicherheitsempfehlungen
CAD Hong Kong issued 9 Safety Recommendations
Issued: -OCT-1996 | To: Pelita Air Service | Safety Recommendation AAR 3-96 (1) |
Pelita Air Service conduct a review of their aircraft and replace any steel wire found being used where copper "tell-tale" wire is specified. (Closed - Acceptable Action) |
Issued: -OCT-1996 | To: Pelita Air Service | Safety Recommendation AAR 3-96 (2) |
Pelita Air Service critically review their company manuals and checklists to ensure that they are consistent, accurate and current. (Closed - Acceptable Action) |
Issued: -OCT-1996 | To: Pelita Air Service | Safety Recommendation AAR 3-96 (3) |
Pelita Air Service re-emphasise the importance of wearing seat belts to their crews. |
Issued: -OCT-1996 | To: Pelita Air Service | Safety Recommendation AAR 3-96 (4) |
Pelita Air Service review their engine and condition control cable maintenance policy for any other Lockheed Hercules aircraft they may have, and consider retrofitting 7 .x 19 CRES control cables with immediate effect. (Closed - Acceptable Action) |
Issued: -OCT-1996 | To: Pelita Air Service | Safety Recommendation AAR 3-96 (5) |
Pelita Air Service review their maintenance management procedures to ensure compliance with the inspection frequency required for engine control cables and cable tension regulators by SMP 515-C-55. |
Issued: -OCT-1996 | To: Pelita Air Service | Safety Recommendation AAR 3-96 (6) |
Pelita Air Service issue appropriate instructions to crews for the arming of emergency lights. (Closed - Acceptable Action) |
Issued: -OCT-1996 | To: HK ATM | Safety Recommendation AAR 3-96 (7) |
Hong Kong Air Traffic Management ensure that the information contained in the emergency alerting list is appropriate and up to date. (Closed - Acceptable Action) |
Issued: -OCT-1996 | To: Lockheed Martin | Safety Recommendation AAR 3-96 (8) |
Lockheed Martin Aeronautical Systems review their advice to operators of the Hercules aircraft in dealing with a suspected throttle control cable failure. (Closed - Acceptable Action) |
Issued: -OCT-1996 | To: Lockheed Martin | Safety Recommendation AAR 3-96 (9) |
Lockheed Martin Aeronautical Systems consider issuing an Alert Service Bulletin recommending change to stainless steel cables for all throttle and condition control cables. |
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Fotos

accident date:
23-09-1994type: Lockheed L-100-30 Hercules
registration: PK-PLV
Map
This map shows the airport of departure and the intended destination of the flight. The line between the airports does
not display the exact flight path.
Distance from Hong Kong-Kai Tak International Airport to Jakarta-Halim Perdana Kusuma Airport as the crow flies is 3258 km (2036 miles).
Accident location: Exact; deduced from official accident report.
This information is not presented as the Flight Safety Foundation or the Aviation Safety Network’s opinion as to the cause of the accident. It is preliminary and is based on the facts as they are known at this time.