Narrative:During maintenance at Maastricht (MST) the right hand main undercarriage was replaced. The landing gear was retracted and deployed several times and performed satisfactory. Prior to being released to the leasing company a test flight was made. During an instrument approach the landing gear was selected down, but the right hand undercarriage did not lock down. The crew recycled the gear and again the right hand main gear came down but failed to lock.
The 'alternate gear extension' procedure was followed but it again failed to lock.
Upon landing the right had undercarriage collapsed.
Probable Cause:
The final report of the investigation did not conform to ICAO Annex 13 standards and did not contain a Probable cause.
It was noted that the hydraulic swivel assembly was connected upside down. This caused the swivel to bend when the landing gear was lowered, preventing it from locking down.
Accident investigation:
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Investigating agency: | Dutch Safety Board  |
Status: | Investigation completed |
Duration: | 3 years and 2 months | Accident number: | 2002086 | Download report: | Final report
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Classification:
Wrong installation of parts
Landing gear collapse
Runway mishap
Photos
Map
This information is not presented as the Flight Safety Foundation or the Aviation Safety Network’s opinion as to the cause of the accident. It is preliminary and is based on the facts as they are known at this time.