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Last updated: 1 May 2017
Statuts:Enquête Officielle
Date:mercredi 1 février 2006
Type/Sous-type:Silhouette image of generic C500 model; specific model in this crash may look slightly different
Cessna 500 Citation I
Compagnie:Flite Services
Immatriculation: N814ER
Numéro de série: 500-0280
Année de Fabrication: 1975
Heures de vol:12008
Moteurs: 2 Pratt & Whitney Canada JT15D-1A
Equipage:victimes: 0 / à bord: 2
Passagers:victimes: 0 / à bord: 2
Total:victimes: 0 / à bord: 4
Dégats de l'appareil: Perte Totale
Conséquences: Written off (damaged beyond repair)
Lieu de l'accident:Burnsville-Mountain Air Airport, NC (   Etats-Unis d'Amérique)
Phase de vol: A l'atterrissage (LDG)
Aéroport de départ:Asheville Municipal Airport, NC (AVL/KAVL), Etats-Unis d'Amérique
Aéroport de destination:Burnsville-Mountain Air Airport, NC, Etats-Unis d'Amérique
The Cessna Citation departed Asheville (AVL) at 11:30 on a 15-minute flight to Burnsville, NC. At Burnsville performed a "touch-and-go." Following the touch-and-go, at about 11:45, and upon raising the landing gear, they got an "unsafe gear" light. The crew cycled the gear back down and got a "three green" normal indication. They cycled the gear back up and again got the "gear unsafe" light. They cycled the gear three more times with the same results. The crew decided to return to Asheville, and upon extending the gear for a visual landing at Asheville, the right main landing gear green light did not illuminate. The crew stated that they performed all of the checklist procedures and asked the control tower personnel to visually look to see if the gear was down and that tower personnel reported that it was. The crew asked the tower personnel if the landing light was on, and tower personnel replied that is was not. According to the flight crew, they went through the emergency procedures again, but they had no luck in getting the landing gear to lock down. They said that there was no landing light and that they got the gear horn with the gear down and full flaps with the throttles at idle. The crew stated they were sure that the gear was out of the uplocks but not down and locked. The crew stated that, after talking with maintenance personnel on the ground at Asheville, they decided to divert to Greensboro/High Point-Piedmont Triad International Airport, NC (GSO), where there were better facilities to handle the situation. One of the passengers had noticed that after the crew had recycled the gear the last time, a panel on the right wing was pushed up. The flight continued to Greensboro, at 150 knots with the gear down. Greensboro tower personnel cleared the flight for a visual approach. According to the crew, the landing was normal for the first 2,000 feet of roll out, then the right main landing gear collapsed. The crew said that, when the gear collapsed, they shut down both engines and the airplane veered off the right side of the runway into the grass. Both crewmembers and passengers exited the airplane through the main door with no injuries.

Probable Cause:

PROBABLE CAUSE: "The pilot's misjudged distance/altitude that led to an undershoot and the pilot's failure to attain the proper touchdown point."



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Ce plan montre l'aéroport de départ ainsi que la supposée destination du vol. La ligne fixe reliant les deux aéroports n'est pas le plan de vol exact.
La distance entre Asheville Municipal Airport, NC et Burnsville-Mountain Air Airport, NC est de 51 km (32 miles).

Les informations ci-dessus ne représentent pas l'opinion de la 'Flight Safety Foundation' ou de 'Aviation Safety Network' sur les causes de l'accident. Ces informations prélimimaires sont basées sur les faits tel qu'ils sont connus à ce jour.
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