ASN Wikibase Occurrence # 322089
Date: | Thursday 12 October 2006 |
Time: | 12:16 |
Type: | Beechcraft 200 Super King Air |
Owner/operator: | Tigress Air III |
Registration: | N528WG |
MSN: | BB-151 |
Year of manufacture: | 1979 |
Total airframe hrs: | 11077 hours |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Destroyed, written off |
Category: | Accident |
Location: | Leonardtown-Saint Mary's County Airport, MD (LTW) -
United States of America
|
Phase: | Landing |
Nature: | Test |
Departure airport: | Leonardtown-Saint Mary's County Airport, MD (LTW) |
Destination airport: | Leonardtown-Saint Mary's County Airport, MD (LTW) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:A Beechcraft 200 Super King Air, N528WG, was destroyed when it suffered a landing accident at Leonardtown-Saint Mary's County Airport, MD (LTW), U.S.
Both occupants were not injured.
The airplane departed Leonardtown Airport to conduct a flight test in the Patuxent River restricted area at approximately 11:15. After approximately one hour, they returned to Leonardtown for a landing.
After entering the traffic pattern for runway 29, the flight crew completed the descent and before landing checklists. The checklists included verifying the landing gear position by visual observation of the landing gear indicator lights, which indicated "three green lights" and no "in-transit" lights. This was also reported over the intercom system to the systems operator, who was seated at his station in the cabin.
After flying the approach to runway 29, the airplane landed on the main gear in a "firm but normal" landing. The airplane touched down approximately 1,200 feet down the runway and within 4 to 5 feet to the right of the runway centerline. Immediately after touchdown, the pilots heard the landing gear warning horn sound intermittently for several seconds, and the right wing began to "drop." The airplane then veered to the right, so the pilot took over the flight controls and attempted to stop the right wing from dropping, but the right propeller struck the runway.
The pilot then moved both fuel condition levers to cutoff, and closed both firewall shutoff valves. The airplane continued to veer right, and the right wing contacted the unimproved grassy area to the right of the pavement, slowing the airplane to a stop. Moments later, the systems operator reported "fire right side," and all three crew members evacuated out of the main cabin door after securing the airplane.
PROBABLE CAUSE: "The airplane manufacturer's inadequate landing gear downlock plate maintenance orientation information, and the disengaged main landing gear."
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC07LA006 |
Status: | Investigation completed |
Duration: | 1 year and 6 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation