Crash-aerien 18 MAR 2010 d'un Antonov An-26B SP-FDO - Tallinn-Ülemiste Airport (TLL)
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Statuts:Accident investigation report completed and information captured
Date:jeudi 18 mars 2010
Heure:10:16
Type/Sous-type:Silhouette image of generic AN26 model; specific model in this crash may look slightly different
Antonov An-26B
Opérant pour:DHL Airways
Loué à :EXIN
Immatriculation: SP-FDO
Numéro de série: 10503
Année de Fabrication: 1980
Heures de vol:25941
Moteurs: 2 Ivchenko AI-24VT
Equipage:victimes: 0 / à bord: 6
Passagers:victimes: 0 / à bord: 0
Total:victimes: 0 / à bord: 6
Dégats de l'appareil: Substantiels
Conséquences: Written off (damaged beyond repair)
Lieu de l'accident:ca 0,3 km W of Tallinn-Ülemiste Airport (TLL) (   Estonie)
Phase de vol: A l'atterrissage (LDG)
Nature:Cargo
Aéroport de départ:Helsinki-Vantaa Airport (HEL/EFHK), Finlande
Aéroport de destination:Tallinn-Ülemiste Airport (TLL/EETN), Estonie
Numéro de vol:EXN3589
Détails:
An Antonov 26B cargo plane sustained substantial damage in a forced landing accident Tallinn-Ülemiste Airport, Estonia following loss of engine power. One of the six occupants was injured.
The flight took off from Helsinki-Vantaa Airport, Finland at 09:46 local time. The flight was uneventful until 10:14 hours, 9.5 nm from Tallinn runway 26. When the power levers were retarded to flight idle the crew noticed engine vibration and smelled a smoke in the cockpit. The engine chip detector indicator in the cockpit was lit. After a short discussion about which engine should be shut down the flight engineer shut down the left engine and the captain tried to start the APU to gain more thrust.
During the approach the air traffic controller noticed the aircraft deviating from the approach path to the left and notified the crew. The crew was unable to maintain a proper approach path both in lateral and vertical dimensions. The attempts to start the APU engine failed. Visual contact with the runway was established 0.5 nm from the threshold. The aircraft crossed the airport boundary being not configured for landing and with an indicated airspeed (IAS) of 295-300 km/h. The flaps were extended for 10° over the threshold; the landing gear was lowered after passing the runway threshold and retracted again.
The aircraft made a high speed low pass over the runway at an altitude of ca 10-15 feet with the landing gear traveling down and up again. Flaps were extended over the runway. At the end of the runway full power on the right engine was selected, and the aircraft climbed 15-20 feet and started turning left. The crew started retracting flaps and lowered the landing gear. The aircraft crossed the highway at the end of the runway at ca 30 feet, then descended again, colliding with treetops at the lake shore and made a crash-landing on the snow and ice-covered lake waterline. Due to the thick ice the aircraft remained on the ice and slid 151 m on the ice with heading 238° before coming to a full stop.
After the impact the flight engineer shoot down the right engine and power and released all engine fire extinguishers. All persons onboard escaped immediately through the main door. No emergency was declared and despite suggestions from first officer, a go-around was not formally commanded.


The airplane gradually sank through the ice after the accident.

Probable Cause:

Causes of the accident:
1. The failure of the left engine lubrication oil system, leading to the failure of the rear compressor bearing and inflight engine failure.
2. The failure of the crew to maintain the approach path and adhere to single engine landing procedures.

Factors contributing to the accident:
1. Improper and insufficient crew training, inter alia complete absence of simulator training
2. The lack of effective coordination between crewmembers
3. The failure of the crew to start RU19A-300 (APU)
4. Adverse weather conditions
5. Inadequate company supervision by Polish CAA, consisting in not noticing the lack of flight crew training and companies generally poor safety culture.
6. Inadequate company maintenance practices, leaving preexisting breather duct failure unnoticed.

Accident investigation:

cover
Investigating agency: ESIB Estonia
Status: Investigation completed
Duration: 2 years and 5 months
Accident number: Final report
Download report: Final report


Opérations de secours

ESIB issued 3 Safety Recommendations

Show all...

Photos

photo of Antonov-An-26B-SP-FDO
accident date: 18-03-2010
type: Antonov An-26B
registration: SP-FDO
 

Video, social media

Plan
Ce plan montre l'aéroport de départ ainsi que la supposée destination du vol. La ligne fixe reliant les deux aéroports n'est pas le plan de vol exact.
La distance entre Helsinki-Vantaa Airport et Tallinn-Ülemiste Airport est de 100 km (63 miles).
Accident location: Exact; deduced from official accident report.

Les informations ci-dessus ne représentent pas l'opinion de la 'Flight Safety Foundation' ou de 'Aviation Safety Network' sur les causes de l'accident. Ces informations prélimimaires sont basées sur les faits tel qu'ils sont connus à ce jour.
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Antonov An-26

  • 1403 built
  • 134ème loss
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 Estonie
  • le accident 7ème le plus grave (à ce moment là)
  • le accident 7ème le plus grave (en ce moment)
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