Accident Tecnam P2002 Sierra N494ES,
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ASN Wikibase Occurrence # 122197
 
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Date:Saturday 16 August 2008
Time:10:05
Type:Silhouette image of generic SIRA model; specific model in this crash may look slightly different    
Tecnam P2002 Sierra
Owner/operator:Private
Registration: N494ES
MSN: 201
Total airframe hrs:51 hours
Engine model:Bombardier-Rotax 912 ULS
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:WOODBINE MUNICIPAL AIRPORT -   United States of America
Phase: Landing
Nature:Training
Departure airport:Woodbine, NJ (1N4)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The student pilot departed and remained in the traffic pattern intending on performing touch-and-go landings. While on final approach with full flaps extended, flying at 10 feet above ground level, the pilot slowed the airplane to 38 knots indicated airspeed (KIAS), though 40 KIAS is the recommended touchdown speed. He reportedly landed, bounced 10 to 15 feet, and applied power to go-around, and he allowed the airplane to decelerate and stall. The airplane was equipped with an electronic flight instrumentation system (EFIS0 that records parameters every 5 seconds including time, date, indicated airspeed, GPS coordinates, ground speed, pitch, pressure altitude, vertical G’s, roll, heading, and slip. Readout of the EFIS revealed the entire accident flight was recorded. Data downloaded from the EFIS indicated that before the airplane stalled the pitch attitude (in degrees) increased to 11.94. The airplane rolled to the left and impacted grass to the left of the runway. There was no preimpact failure or malfunction of the airplane or its systems. The 75 hour student pilot stated that he was under stress due to an issue related to work, and he should not have been flying that day. He also reported, "he was much less focused than he should have been."
Probable Cause: The student pilot's failure to maintain airspeed during a go-around. Contributing to the accident was the student pilot's degraded emotional/mental state due to stress.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA08LA166
Status: Investigation completed
Duration: 1 year and 2 months
Download report: Final report

Sources:

NTSB

Location

Media:

Revision history:

Date/timeContributorUpdates
09-May-2011 15:08 StreetF117 Added
21-Dec-2016 19:25 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
03-Dec-2017 11:58 ASN Update Bot Updated [Cn, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative]

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