Accident Beechcraft H35 Bonanza N375B,
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ASN Wikibase Occurrence # 152237
 
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Date:Friday 4 January 2013
Time:14:19
Type:Silhouette image of generic BE35 model; specific model in this crash may look slightly different    
Beechcraft H35 Bonanza
Owner/operator:Private
Registration: N375B
MSN: D-5121
Year of manufacture:1957
Engine model:Continental IO-470 SERIES
Fatalities:Fatalities: 3 / Occupants: 3
Aircraft damage: Destroyed
Category:Accident
Location:East of Flagler County Airport - KXFL, Palm Coast, FL -   United States of America
Phase: Approach
Nature:Private
Departure airport:St.Lucie County, FL (FPR)
Destination airport:Knoxville, TN (DKX)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airplane departed under visual flight rules and was at an altitude of about 7,500 feet when the pilot reported vibrations and an “oil pressure problem.” Airports in the area were under instrument meteorological conditions with cloud ceilings of 900 to 1,000 feet above ground level (agl). An air traffic controller provided the pilot with radar vectors for an airport surveillance radar (ASR) approach to a nearby airport that did not have a published ASR procedure. The airplane was about 2.5 miles northwest of the airport, at an altitude of about 5,300 feet agl, when the pilot reported that the engine oil pressure was “zero” with “cool cylinders.” The controller did not obtain nor did the pilot provide any additional information about the engine’s power status. During the next approximately 7 minutes, the airplane continued past the airport to a point about 6.5 miles northeast before the controller vectored the airplane to the south and then west to the final approach course. The airplane subsequently struck trees and a residence about 3/4 mile from the approach end of the runway. A postcrash fire destroyed the airframe and engine.
Postaccident examination of the airplane revealed that the engine sustained a fractured No. 4 connecting rod due to oil starvation. The connecting rod punctured the crankcase, which resulted in a total loss of engine power. The crankshaft oil transfer passage at the No. 4 journal sustained mechanical damage during the accident sequence and contained displaced journal material. All other oil passages were unrestricted. The airplane’s maintenance logbooks were destroyed during the accident. Maintenance performed on the airplane about 1 month before the accident included the replacement of the Nos. 1 and 4 cylinders; however, it could not be determined if this maintenance played a role in the accident. The reason for the oil starvation could not be determined.
Review of the air traffic control transcripts and interviews with the controllers revealed that they vectored the airplane such that it was unable to reach the airport. This was likely due to the weather conditions and the controllers’ incomplete understanding of the airplane’s mechanical condition (complete loss of power), which the pilot did not provide.
At the time of the accident, the pilot was using medication for hypertension and had well-controlled diabetes. It was unlikely that either condition significantly affected the pilot’s performance at the time of the accident.

Probable Cause: A total loss of engine power after the failure of the No. 4 connecting rod due to oil starvation, which resulted in a subsequent forced landing. Contributing to the accident was the pilot’s failure to clearly state that the aircraft had lost all power and the air traffic controllers’ incomplete understanding of the emergency, which resulted in the controllers vectoring the airplane too far from the airport to reach the runway.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA13FA105
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB
FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=375B

Location

Revision history:

Date/timeContributorUpdates
04-Jan-2013 19:04 Geno Added
05-Jan-2013 00:08 Alpine Flight Updated [Aircraft type]
21-Dec-2016 19:28 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
28-Nov-2017 14:05 ASN Update Bot Updated [Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative]

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