ASN Wikibase Occurrence # 172643
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Date: | Sunday 21 December 2014 |
Time: | 10:30 |
Type: | ASAP Beaver RX550 |
Owner/operator: | Private |
Registration: | N105JF |
MSN: | 105 |
Year of manufacture: | 2006 |
Total airframe hrs: | 618 hours |
Engine model: | Rotax 528 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Perris Valley Airport (L65), Perris, CA -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Perris, CA (L65) |
Destination airport: | Perris, CA (L65) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The private pilot, who was also the owner/builder of the experimental, amateur-built light sport airplane, was conducting a personal flight. The pilot reported that, earlier on the morning of the accident, he had conducted the first flight since he had performed some maintenance to resolve a longstanding engine surging problem and that, during that flight, the engine operated normally.
During takeoff for the accident flight, the engine initially performed normally, but when the pilot initiated the crosswind turn, the engine started to make a “hollow” sound, accompanied by a partial loss of power. As the pilot attempted to maneuver the airplane away from power lines during the attempted forced off-field landing, he lost airplane control, which resulted in an aerodynamic stall and impact with terrain.
Postaccident examination revealed numerous installation and maintenance discrepancies related to the carburetor and fuel supply system, which were not in accordance with the engine manufacturer’s installation and maintenance manuals. Any one of these discrepancies could have resulted in the loss of engine power.
Probable Cause: The partial loss of engine power during takeoff due to an improperly configured carburetor and fuel supply system. Contributing to the accident was the pilot's loss of airplane control during the off-field landing, which resulted in an aerodynamic stall.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR15LA067 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=N105JF Location
Revision history:
Date/time | Contributor | Updates |
03-Jan-2015 03:58 |
Geno |
Added |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
30-Nov-2017 19:43 |
ASN Update Bot |
Updated [Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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