ASN Wikibase Occurrence # 188559
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Date: | Thursday 7 July 2016 |
Time: | 12:00 |
Type: | Piper PA-44-180 Seminole |
Owner/operator: | Plane Nonsense Inc |
Registration: | N190ND |
MSN: | 4495002 |
Year of manufacture: | 1989 |
Total airframe hrs: | 9927 hours |
Engine model: | Lycoming LO-360-A1H6 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Dillant-Hopkins Airport (KEEN), Keene, NH -
United States of America
|
Phase: | Landing |
Nature: | Training |
Departure airport: | Bedford, MA (BED) |
Destination airport: | Keene, NH (EEN) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The flight instructor in the multiengine airplane reported that, during a simulated single-engine instrument approach to runway 2, the right engine was configured for the simulated failure. The instructor added that the goal was to perform a missed approach on one engine and note the airplane’s performance. The pilot under instruction descended to the decision height and executed the missed approach procedure, but the airplane would not climb. The flight instructor told the pilot to go to full power on both engines. According to the flight instructor, “mixtures, props and throttles were all full forward and the fuel flow levers were both at the ON position,” and he took control of the airplane.
The flight instructor reported that there were trees and buildings to the north and that he made a left turn about 400 ft above ground level with the intent to land on runway 14. He extended the landing gear but realized that he would not reach the runway. He executed a forced landing to the southwest on taxiway Sierra, the airplane crossed over runway 32/14, and although heavy braking was applied, the airplane exited the taxiway and impacted a drainage culvert. The airplane sustained substantial damage to the aft fuselage stringers and longerons.
The airport elevation was 488 ft, the density altitude was 2,120 ft, the temperature was 81°, the dew point was 66° F, and the wind was calm, and the flight instructor stated that carburetor heat was not used during the approach on either engine.
The relative humidity was about 60 percent, and the weather conditions were conducive to serious icing probability when operating in a gliding flight profile.
Probable Cause: The flight instructor’s failure to use carburetor heat during the approach while operating in atmospheric conditions that were conducive to carburetor icing, which resulted in a loss of engine power due to carburetor icing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | GAA16CA377 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=190ND https://flightaware.com/live/flight/N190ND
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
08-Jul-2016 04:15 |
Geno |
Added |
19-Aug-2017 14:15 |
ASN Update Bot |
Updated [Time, Total occupants, Other fatalities, Nature, Departure airport, Destination airport, Source, Damage, Narrative] |
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