Accident Piper PA-28-180 Cherokee N9427J,
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ASN Wikibase Occurrence # 196518
 
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Date:Tuesday 4 July 2017
Time:17:21
Type:Silhouette image of generic P28A model; specific model in this crash may look slightly different    
Piper PA-28-180 Cherokee
Owner/operator:Horizon Aviation
Registration: N9427J
MSN: 28-3538
Year of manufacture:1966
Total airframe hrs:4323 hours
Engine model:Lycoming O-360-A3A
Fatalities:Fatalities: 0 / Occupants: 4
Aircraft damage: Substantial
Category:Accident
Location:Isla Grande Airport, San Juan -   Puerto Rico
Phase: Take off
Nature:Private
Departure airport:San Juan-Fernando Luis Ribas Dominicci Airport (SIG/TJIG)
Destination airport:San Juan-Fernando Luis Ribas Dominicci Airport (SIG/TJIG)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The private pilot reported that, before the local, personal flight, the airplane was fueled and that he performed a preflight inspection and an engine run-up with no issues noted. The takeoff was normal; however, during the initial climb, about 250 ft above ground level, the engine started to run roughly and lose power. The engine did not respond to throttle inputs. The pilot contacted the air traffic control tower and stated that he intended to return to the departure airport to land. He did not recall the remainder of the accident sequence. A passenger, who was also a certificated pilot, stated that, as the pilot was turning the airplane left back to the airport, he saw that the airspeed was decreasing and that the stall warning light was flashing. Subsequently, the airplane entered an aerodynamic stall and spun into a canal. A review of a video taken by a witness corroborated the passenger's account.
Examination of the airframe and engine did not reveal any preaccident mechanical malfunctions or failures that would have precluded normal operation. Sound spectrum analysis of onboard video revealed that the engine rpm decreased by about 300 and then increased by about 300 twice but then remained steady near full power for about 6 seconds before impact. The reason for the rpm changes could not be determined.

Probable Cause: A partial loss of engine power during initial climb for reasons that could not be determined and the pilot's subsequent exceedance of the airplane's critical angle of attack, which resulted in an aerodynamic stall.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA17LA227
Status: Investigation completed
Duration: 2 years and 9 months
Download report: Final report

Sources:

NTSB

Location

Media:

Revision history:

Date/timeContributorUpdates
05-Jul-2017 02:09 Geno Added
05-Jul-2017 12:04 Iceman 29 Updated [Aircraft type, Registration, Cn, Operator, Nature, Source, Embed code]
05-Jul-2017 12:09 Iceman 29 Updated [Embed code, Narrative]
05-Jul-2017 16:54 harro Updated [Registration, Source, Narrative]
22-Apr-2020 17:00 ASN Update Bot Updated [Time, Operator, Country, Nature, Departure airport, Destination airport, Source, Embed code, Narrative, Accident report, ]
22-Apr-2020 17:19 harro Updated [Aircraft type, Embed code, Narrative, Accident report, ]
20-Sep-2023 06:54 Ron Averes Updated [[Aircraft type, Embed code, Narrative, Accident report, ]]

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