Fuel exhaustion Accident Beechcraft 58TC Baron N2CH,
ASN logo
ASN Wikibase Occurrence # 198815
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Saturday 5 November 2016
Time:16:43
Type:Silhouette image of generic B58T model; specific model in this crash may look slightly different    
Beechcraft 58TC Baron
Owner/operator:H3 Aviation, LLC
Registration: N2CH
MSN: TK-72
Year of manufacture:1978
Total airframe hrs:4654 hours
Engine model:Continental TSIO-520-WB
Fatalities:Fatalities: 0 / Occupants: 3
Aircraft damage: Substantial
Category:Accident
Location:Valdosta, GA -   United States of America
Phase: En route
Nature:Private
Departure airport:Columbia, SC (KCAE)
Destination airport:Quitman, GA (4J5)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
According to the pilot of the twin-engine airplane, he descended from 7,000 ft and leveled off at 3,000 ft. After leveling off, the fuel quantity indicators fluctuated then showed empty. He recalled that, about 5 minutes after leveling off, the right engine began to run very roughly, so he enriched the right engine’s mixture and activated the auxiliary fuel pump. He added that, subsequently, “the right engine failed and the left engine simultaneously began losing power.” The pilot declared an emergency with air traffic control, began receiving vectors, and the left engine lost power.
The pilot pitched the airplane for best glide distance. He selected the nearest suitable landing area, extended the landing gear and flaps, and landed the airplane in a field. During the landing roll, he turned the airplane to the right to avoid a collision with obstacles, and the nose landing gear bounced several times and separated from the airplane. The airplane sustained substantial damage to the fuselage bulkheads, longerons, and stringers.
The pilot believed that, due to his failure to visually check the fuel level, he overestimated the amount of fuel on board.
The pilot reported that there were no preaccident mechanical malfunctions or failures with the airplane that would have precluded normal operation.


Probable Cause: The pilot’s failure to ensure that adequate fuel was onboard for the flight, which resulted in fuel exhaustion and the loss of engine power.


Accident investigation:
cover
  
Investigating agency: NTSB
Report number: GAA17CA058
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB

Location

Revision history:

Date/timeContributorUpdates
19-Aug-2017 15:11 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org