ASN Wikibase Occurrence # 208618
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Date: | Saturday 29 July 2017 |
Time: | 18:30 |
Type: | Mooney M20C |
Owner/operator: | Private |
Registration: | N2596W |
MSN: | 3283 |
Year of manufacture: | 1965 |
Engine model: | Lycoming O&VO-360 SER |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Clearwater, FL -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Clearwater, FL (CLW) |
Destination airport: | Clearwater, FL (CLW) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that he extended the landing gear while in the traffic pattern. He added that he became distracted by a helicopter that was transitioning to the airport, and while on base to final approach, he mistakenly raised the landing gear. The airplane subsequently touched down with the landing gear retracted.
The fuselage sustained substantial damage.
The pilot reported that there were no preaccident mechanical malfunctions or failures with the airplane that would have precluded normal operation.
Probable Cause: The pilot’s distraction before landing by a helicopter that was transitioning to the airport and his subsequent failure to extend the landing gear before touchdown.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | GAA17CA481 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
02-Apr-2018 07:34 |
ASN Update Bot |
Added |
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