ASN Wikibase Occurrence # 245856
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Date: | Saturday 19 December 2020 |
Time: | 15:30 LT |
Type: | Sonex Aircraft Sonex |
Owner/operator: | Private |
Registration: | N935EK |
MSN: | 1617 |
Year of manufacture: | 2019 |
Engine model: | AeroVee |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | near Fort Worth Spinks Airport (FWS/KFWS), Fort Worth, TX -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Burleson, TX |
Destination airport: | Burleson, TX |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot and builder of the airplane was conducting the airplane's first flight. The pilot contacted the tower controller and requested to orbit the airport for 30 minutes at 3,500 ft. Shortly after departure, the pilot reported that he was unable to climb and needed to return to the airport. The pilot reported that he had a 'sick engine,' and he was 'just trying to make the field.' The controller reported to the pilot that smoke appeared to be coming from the engine.
Automatic Dependent Surveillance'“Broadcast (ADS-B) data revealed the airplane departed from the airport, turned, and flew south for about 2 miles before it turned north back to the airport. During the subsequent forced landing, the airplane impacted powerlines and terrain and came to rest inverted about 1 mile south of the airport.
During the engine examination oil was present on the dipstick. The oil filter was cut open and fine metal pieces/powder were observed on the filter element, and small metal pieces were observed in the engine's oil filter port. The engine was seized and could not be rotated by hand. The engine was not dissembled further, and the source of the metal filings was not determined.
The loss of engine power was attributed to the seizure of the engine; however, the reason for the engine seizure could not be determined. Investigators were unable to determine why the pilot did not stay over the airport and orbit as originally requested.
Probable Cause: A total loss of engine power due to engine seizure. Contributing to the accident was the pilot decision not to orbit the airport, as originally planned.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN21LA092 |
Status: | Investigation completed |
Duration: | 1 year and 6 months |
Download report: | Final report |
|
Sources:
NTSB CEN21LA092
https://flightaware.com/live/flight/N935EK FAA register:
https://registry.faa.gov/aircraftinquiry/Search/NNumberResult Location
Revision history:
Date/time | Contributor | Updates |
20-Dec-2020 02:50 |
Geno |
Added |
20-Dec-2020 02:52 |
Geno |
Updated [Aircraft type, Location] |
20-Dec-2020 09:49 |
Anon. |
Updated [Nature] |
15-Jul-2022 11:02 |
ASN Update Bot |
Updated [Time, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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