Accident Cessna 150K N6098G,
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ASN Wikibase Occurrence # 296306
 
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Date:Friday 3 January 2003
Time:09:12 LT
Type:Silhouette image of generic C150 model; specific model in this crash may look slightly different    
Cessna 150K
Owner/operator:Private
Registration: N6098G
MSN: 15071598
Year of manufacture:1969
Total airframe hrs:3569 hours
Engine model:Continental O-200A
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Jessup, Georgia -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Brunswick-Malcolm McKinnon Airport, GA (SSI/KSSI)
Destination airport:Macon-Lewis B. Wilson Airport, GA (MCN/KMCN)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot stated that the flight departed with full fuel tanks (26 gallons total) and approximately 40 minutes into the flight while flying at 2,400 feet mean sea level, the engine rpm decreased suddenly from 2,400 to 1,500. The engine continued to operate at 1,500 rpm and was running smoothly. Carburetor heat was applied and the throttle and mixture controls were manipulated with no response; the engine rpm remained at 1,500. He communicated with Macon Automated Flight Service Station and advised of the loss of engine power and of an impending off field landing. He maneuvered the airplane for a landing on a service road among a large area of small pines trees, and during flare to land, the left wing tip contacted a 3-inch diameter tree trunk which was not visible during the approach. The airplane cart wheeled to the left, and the nose landing gear separated after contacting soft ground. The airplane then nosed over and the pilot exited the airplane from the left door which had popped open. He later stated that he did not see any fuel leakage after exiting the airplane. He estimated the airplane remained inverted for approximately 24 hours. According to the Macon, Georgia, Automated Flight Service Station quality assurance manager, the pilot activated his VFR flight plan while airborne between 0830 and 0832, and contacted the facility again while airborne at 0910. At the second contact he advised of having a fuel problem and was losing altitude. The pilot contacted the facility again using a cellular phone at 0942 hours. NTSB review of the tape of the in-flight contact with Macon AFSS revealed the pilot did in fact advise he was having a fuel problem and was losing altitude. The FAA did not examine the airplane at the scene. According to the FAA inspector who examined the airplane following recovery, both fuel tank caps were loose when installed, and the fuel vent diaphragm of the right wing fuel cap was observed to be torn. Aft streaking of fuel from both fuel caps was noted; the fuel cap seals were poor. There was only residual fuel noted in both fuel tanks, the amount was not quantified. The gascolator bowl was found to only have 1/4 inch of fuel, while the carburetor bowl was empty. A differential compression test was performed before an attempted engine run; cylinders 1, 3, and 4, were recorded to be 76 or better when tested against 80 psi. The No. 2 cylinder differential compression check was 12 psi. The engine run was performed on airframe with the accident propeller installed; the impact damaged propeller was straightened for the attempted engine run. The engine was started and operated to approximately 2,000 rpm; no discrepancies were noted during the engine run. Magneto checks performed at idle indicate each dropped 75 rpm, and the oil pressure was 45 psi during the run. Safety concerns prevented operation at a higher rpm. Examination of photographs taken of the airplane at the scene revealed the leading edges of both wings was at a lower elevation than the trailing edges.

Probable Cause: The loss of engine power for undetermined reasons. A contributing factor was unsuitable terrain.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA03LA044
Status: Investigation completed
Duration: 1 year and 3 months
Download report: Final report

Sources:

NTSB MIA03LA044

Revision history:

Date/timeContributorUpdates
13-Oct-2022 19:04 ASN Update Bot Added

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