Accident Piper PA-24-250 N328EJ,
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ASN Wikibase Occurrence # 297667
 
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Date:Sunday 13 January 2002
Time:14:37 LT
Type:Silhouette image of generic PA24 model; specific model in this crash may look slightly different    
Piper PA-24-250
Owner/operator:
Registration: N328EJ
MSN: 24-2356
Year of manufacture:1960
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Oceano, California -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Oceano, CA (L52)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airplane lost engine power in the traffic pattern and collided with an airport perimeter fence when it landed short of the runway. The pilot reported that while on the downwind leg of the traffic pattern, he lowered the landing gear. He heard a loud bang from the firewall area, and the instrument panel caved in. The engine lost power, and he maneuvered the airplane towards the airport. The airplane touched down about 500 to 1,000 feet short of the runway, and collided with an airport perimeter fence. A post accident examination of the airplane revealed that the mixture control cable separated at the mixture control arm. The engine control bracket, part number 21189-00, was missing. Without the bracket, the mixture control cable hangs freely down below the engine, where the nose gear is located when in the retracted position. A kink in the mixture cable indicated that it became caught on a Zerk fitting located on the pivot point of the nose landing gear when the nose gear was extended to the down position. This resulted in the mixture control cable separating from the mixture control arm on the carburetor. Maintenance records revealed that the airplane was about 2 months overdue for an annual inspection.

Probable Cause: A loss of engine power due to the separation of the mixture control cable from the mixture control arm of the carburetor. The mixture cable separation was due to maintenance personnel's failure to secure the mixture control cable away from the nose landing gear, which resulted in the cable snagging during gear extension. A factor in the accident was the airplane being overdue for an annual inspection.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: 
Status: Investigation completed
Duration: 2 years and 8 months
Download report: Final report

Sources:

NTSB LAX02LA065

Revision history:

Date/timeContributorUpdates
15-Oct-2022 07:03 ASN Update Bot Added

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