ASN Wikibase Occurrence # 38105
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Tuesday 21 November 1989 |
Time: | 21:43 |
Type: | Piper PA-28-235 |
Owner/operator: | Harris Int'l Flying Club |
Registration: | N9465W |
MSN: | 28-11189 |
Fatalities: | Fatalities: 3 / Occupants: 3 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Monroe Center, IL -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Rockford, IL (RFD) |
Destination airport: | Bloomington, IL (BMI) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:NON-INSTRUMENT RATED PRIVATE PILOT TOOK OFF IN IMC CONDITIONS AT NIGHT; CRASHED 9 MINUTES LATER. WITNESSES REPORTED SEEING THE AIRCRAFT IN A STEEP DIVE, ON FIRE, PRIOR TO IMPACT. EXTENSIVE FIRE DAMAGE INTERIOR CABIN. NO EVIDENCE OF INSULATION GROMMET AT FRAME PENETRATION OF MAIN WIRING HARNESS, OR CABLE INSULATION FROM THIS POINT TO BATTERY. BATTERY BOX BULGED OUT ALL SIDES, BLACK & CHARRED. WING SPAR WEB MELTED AND MISSING FROM WHERE ELECT FUEL PUMP ATTACHES TO SPAR TO RIGHT SIDE WING ATTACH POINT. ALUM WIRING REPLACED DURING LAST ANNUAL 4/29/89. LOG SHEET ENTRY 11/18/89 'BAD GAS SMELL!'. CAUSE: IN-FLIGHT FIRE INITIATED BY AN INADEQUATELY INSTALLED WIRING HARNESS AND PROPAGATED BY AN EXISTING FUEL LEAK WHICH WAS NOT REPAIRED.
Sources:
NTSB:
https://www.ntsb.gov/ntsb/brief.asp?ev_id=20001213X29759 Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation