Accident Glasair N59LP,
ASN logo
ASN Wikibase Occurrence # 39502
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Tuesday 2 April 1996
Time:11:58 LT
Type:Silhouette image of generic GLAS model; specific model in this crash may look slightly different    
Glasair
Owner/operator:Bobby A. Hockett
Registration: N59LP
MSN: 156
Total airframe hrs:1656 hours
Engine model:Lycoming O-360-A1G
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Destroyed
Category:Accident
Location:Groveland, CA -   United States of America
Phase: En route
Nature:Private
Departure airport:(Q68)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot (part owner of the aircraft) held an A&P certificate & had completed a condition/annual inspection of the aircraft before the flight. The aircraft co-owner stated there was a problem with the throttle cable, & the pilot was going to order a new one, but had not yet done so. Witnesses said the aircraft departed straight out after takeoff. About 4 minutes later, it entered a downwind to the pattern, low & very close to the runway. The witnesses estimated the aircraft's altitude was between 200 and 300 feet agl. At first, some witnesses thought the pilot was going to make a downwind landing on the runway. The witnesses said the aircraft made a tight turn from downwind to base. During the base-to-final turn, the right wing dropped, and the aircraft entered a nose-down descent and crashed. The witnesses heard the engine running before impact, but they described the sound as 'not full power.' An examination of the engine & controls revealed that a clip, which secured the accelerator pump plunger to its actuation shaft in the carburetor, was missing & the pump was inoperative. The throttle cable housing/actuating shaft at the carburetor end was found separated from the cable sheath, exposing the unsupported inside cable. A piece of welding rod was found bent around the housing end & taped to the sheath. The cable was removed from the aircraft & operationally tested. During push-pull tests, the carburetor end would sometimes move an amount corresponding to the cockpit end input; at other times, the carburetor end would move only slightly.

Probable Cause: the pilot's decision to fly the aircraft with a known mechanical discrepancy in the throttle linkage, which resulted in a partial loss of engine power; and his failure to maintain an adequate airspeed while maneuvering for an emergency landing, which resulted in an inadvertent stall/spin. Inadequate maintenance/annual inspection was a related factor.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX96LA152
Status: Investigation completed
Duration: 10 months
Download report: Final report

Sources:

NTSB LAX96LA152

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:23 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
09-Apr-2024 07:38 ASN Update Bot Updated [Time, Operator, Other fatalities, Source, Narrative, Category, Accident report]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org