ASN Wikibase Occurrence # 40515
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Friday 25 June 1993 |
Time: | 12:30 |
Type: | Mooney M20K |
Owner/operator: | private |
Registration: | N5655M |
MSN: | 25-0758 |
Year of manufacture: | 1983 |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Hobart, IN -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | (3HO) |
Destination airport: | Unknown |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE AIRPLANE WAS OBERVED DEPARTING IN LIGHT MIST BY THE AIRPORT MANAGER AND THREE OTHER PERSONS. THE AIRPLANE WAS OVERDUE AND A SEARCH WAS CONDUCTED BY THE CIVIL AIR PATROL AND THE U.S. COAST GUARD. THE SOUTHERN PORTION OF LAKE MICHIGAN AND SURROUNDING LAND MASS WAS SEARCHED WITH NEGATIVE RESULTS. APPROXIMATELY ONE WEEK PRIOR TO THE MISSING AIRPLANE'S DEPARTURE AN EMPLOYEE OF THE PILOT WAS DIRECTED BY THE PILOT TO CHANGE THE VACUUM PUMP. THE MECHANIC WAS NOT ABLE TO DO SO. THE MECHANIC STATED THE PILOT TOLD HIM HE HAD REMOVED THE PUMP LATER IN THE WEEK. NO EVIDENCE OF SUCH MAINTENANCE WAS FOUND DURING THE INVESTIGATION. PIECES OF AN AIRPLANE HAVE BEEN FOUND ALONG THE MICHIGAN LAKESHORE WHICH MATCH THE AIRPLANE'S INTERIOR AND EXTERIOR COLORS. THE PILOT IS PRESUMED DEAD. CAUSE: undetermined.
Sources:
NTSB:
http://www.ntsb.gov/ntsb/brief.asp?ev_id=20001211X12554 Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation