Accident Piper PA-46-310P Malibu N4386G,
ASN logo
ASN Wikibase Occurrence # 44440
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Monday 4 July 2005
Time:17:58
Type:Silhouette image of generic PA46 model; specific model in this crash may look slightly different    
Piper PA-46-310P Malibu
Owner/operator:Private
Registration: N4386G
MSN: 46-8508037
Year of manufacture:1985
Total airframe hrs:1856 hours
Engine model:Teledyne Continental TSIO-520-BE1
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Destroyed
Category:Accident
Location:Grand Rapids, MN -   United States of America
Phase: Landing
Nature:Private
Departure airport:Grand Rapids, MN (GPZ)
Destination airport:Minneapolis, MN (FCM)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airplane was destroyed on impact with terrain during a forced landing following an observed in-flight loss of engine power after takeoff. A witness observed the takeoff and stated that the airplane took off from the end of runway 34. About halfway down the runway the airplane emitted a sound like a rapid misfire, a pop, and then no more audible engine sounds. The airplane was about 300 to 400 feet above ground level at that point. He said that the airplane turned right then turned left to a bank where the wing was straight down. The airplane's wings then leveled, the airplane descended, and it impacted terrain. He stated that the time from the sounds to the impact was about two to three seconds. An on-scene examination revealed no airframe pre-impact anomalies. An engine examination revealed a cracked crankshaft propeller flange. The engine without the turbochargers and with the original crankshaft was test run up to 2,100 RPM. A propeller and governor inspection revealed no anomalies. Examination of the turbocharger system's exhaust bypass valve assembly revealed its butterfly valve was stuck (bound) in the extended closed position. The engine's cracked crankshaft was removed and a serviceable crankshaft was installed. The engine was test run again with a serviceable exhaust bypass valve assembly. The engine produced rated power. The original exhaust bypass valve assembly was reinstalled. The exhaust bypass valve assembly's wastegate bound again during an engine run and a loss of engine power was observed. Sectioning of the bypass valve assembly revealed a bent wastegate shaft. The valve assembly lever arm was bent and exhibited pre-impact toolmarks consistent with pliers loosening a bound wastegate shaft. The airplane's pilot operating handbook and Federal Aviation Administration (FAA) approved airplane flight manual (POH), in part, stated, "ENGINE POWER LOSS DURING TAKEOFF If sufficient runway remains for a normal landing, leave gear down and land straight ahead." The engine manufacturer's maintenance and operator's manual stated that the wastegate is required to be checked for operation and condition during 100 hour inspections. The manual did not specify a procedure for maintenance personnel on how to check the wastegate's operation and its acceptable condition. National Transportation Safety Board Recommendation A-94-081, issued to the FAA in 1994, stated, "Require the amendment of pilot operating handbooks and airplane flight manuals applicable to aircraft equipped with engine turbochargers by including in the 'Emergency Procedures' section information regarding turbocharger failure. The information should include procedures to minimize potential hazards relating to fire in flight and/or loss of engine power." The airplane's POH latest revision was dated October 14, 2002 and review of the emergency procedures section showed that the POH did not contain information, procedures, or amplified procedures on turbocharger failures. The airplane accumulated 8.7 hours of operation since the last annual inspection.
Probable Cause: An observed loss of engine power due to the bound/jammed turbocharger wastegate during takeoff, the pilot not maintaining airplane control, and the stall he inadvertently encountered. A factor was the maintenance personnel not replacing the turbocharger wastegate bypass valve assembly during the last annual inspection 8.7 hours of operation prior to the accident. An additional factor was the manufacturer's insufficiently defined inspection conditions for the bypass valve's proper operation.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CHI05FA162
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20050711X00980&key=1

History of this aircraft

Other occurrences involving this aircraft
6 July 2003 N4386G 0 Englewood, Colorado sub

Location

Revision history:

Date/timeContributorUpdates
28-Oct-2008 00:45 ASN archive Added
21-Dec-2016 19:24 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
06-Dec-2017 10:42 ASN Update Bot Updated [Operator, Destination airport, Source, Narrative]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org