Accident Socata TB20 Trinidad N575RM,
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ASN Wikibase Occurrence # 45403
 
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Date:Thursday 3 October 2002
Time:09:32
Type:Silhouette image of generic TB20 model; specific model in this crash may look slightly different    
Socata TB20 Trinidad
Owner/operator:Douglas K. White
Registration: N575RM
MSN: 575
Total airframe hrs:2593 hours
Engine model:Lycoming IO-540-C4D5D
Fatalities:Fatalities: 1 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:Texarkana, AR -   United States of America
Phase: Manoeuvring (airshow, firefighting, ag.ops.)
Nature:Training
Departure airport:Texarkana, AR (TXK)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The flight was returning to the airport so the student pilot could practice a few landings, including a practice engine-out approach and landing. During the practice simulated engine-out landing, the airplane's left wing struck the ground while turning toward the runway. A witness reported observing the airplane make a turn, and it appeared to be paralleling the runway while continuing "to descend to 500 feet agl or less." At an altitude of 200 or 300 feet agl, the "aircraft rolled into a 60 to 80 degree banked left turn" toward the runway. The airplane appeared to "stall," and the left wing impacted the ground. The witness further reported that "at no time did [he] hear an engine noise or any changes in power from what seemed to be power-off or idle power." The flight instructor reported that the left turn and bank looked like a "normal" standard rate turn at the beginning, but it "suddenly became very steep." The flight instructor stated that she had reminded the student "that even if we were doing the practice engine out procedure back to the runway, that he could add power back if he felt we were getting too low." According to the flight instructor the flight was in preparation for the student pilot to take the single-engine land airplane private pilot examination. No structural or mechanical anomalies were observed during an examination of the airplane.
Probable Cause: The inadvertamt stall by the student pilot, and the inadequate supervision by the flight instructor.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: FTW03FA003
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20021010X05304&key=1

Location

Revision history:

Date/timeContributorUpdates
28-Oct-2008 00:45 ASN archive Added
21-Dec-2016 19:24 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
09-Dec-2017 17:55 ASN Update Bot Updated [Source, Narrative]

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