ASN Wikibase Occurrence # 131532
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Date: | Saturday 18 June 2011 |
Time: | 13:00 |
Type: | Cessna 172P Skyhawk |
Owner/operator: | Private |
Registration: | N65654 |
MSN: | 17275800 |
Year of manufacture: | 2005 |
Total airframe hrs: | 1645 hours |
Engine model: | Lycoming IO-360-L2A |
Fatalities: | Fatalities: 0 / Occupants: 5 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Near Mt. Pleasant, about 60 miles south of Salt Lake City, UT -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Mount Pleasant, UT (43U) |
Destination airport: | Mount Pleasant, UT (43U) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:On the day of the accident, the pilot reported that he expected the borrowed airplane’s fuel tanks to be full. Since there was no ladder available to visually view the fuel tank quantity or to use a dip stick, he relied on the fuel gauges, which indicated that the left tank was about 3/8 full and the right fuel gauge indicated full. After accomplishing two parachute drops, an individual asked the pilot to take him and his children on a local sightseeing flight. During that flight, the engine lost power and the pilot subsequently made a forced landing to a field. During the wreckage recovery, personnel reported that neither fuel tank was breached and that the tanks were empty, suggesting that the loss of engine power was due to fuel exhaustion. Throughout the day, the airplane’s fuel quantity gauges gave indications that suggested the tanks contained fuel, and the pilot, therefore, continued to fly the airplane without visually inspecting the quantity of fuel in the tanks. Postaccident examination and testing of the fuel quantity indicating system did not reveal any mechanical malfunctions or failures that would preclude normal operation. The pilot who previously flew the airplane reported that, although the protocol was that all individuals who borrowed the airplane were to fill its fuel tanks after using it, he had failed to do so and left about 5 gallons of fuel in one tank and about 3 gallons of fuel in the other.
Probable Cause: The pilot’s failure to determine the airplane’s fuel quantity before takeoff, which resulted in a loss of engine power due to fuel exhaustion.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR11LA266 |
Status: | Investigation completed |
Duration: | 1 year and 5 months |
Download report: | Final report |
|
Sources:
NTSB
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
18-Jun-2011 23:38 |
gerard57 |
Added |
19-Jun-2011 04:54 |
RobertMB |
Updated [Aircraft type, Registration, Cn, Operator, Location, Source, Damage, Narrative] |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
27-Nov-2017 16:55 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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