ASN Wikibase Occurrence # 131814
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Date: | Sunday 11 June 2000 |
Time: | 10:35 |
Type: | Cessna 150M |
Owner/operator: | Private |
Registration: | N66081 |
MSN: | 15075821 |
Year of manufacture: | 1974 |
Total airframe hrs: | 4850 hours |
Engine model: | Continental O-200-A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Bethalto, IL -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Greensburg, IN (I34) |
Destination airport: | ST CLAIR, MO (K39) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:N66081 was destroyed when it nosed over on impact with a ditch during a forced landing following an in-flight loss of engine power. The pilot was uninjured. The pilot said, 'I preflighted the airplane at 6:45 a.m. and checked fuel prior to take off from I34. The airplanes was fueled the day prior and flown .5 hrs or less.' The pilot stated, 'While enroute to (K39) St.Clair Regional I decided to stop at (VLA) Vandalia, IL for a weather update and restroom break. ... Vandalia had 2 parachutists under canopy and two more jumping in less that 2 minutes. The traffic pattern was full as well so I decided to fly northeast to St. Louis Regional - get fuel and a weather briefing. After getting clearance to land and setting up for pattern entry and starting to level off from descent to traffic pattern altitude the engine quit running. I radioed the tower and squacked 7700 on the x-ponder. After all emergency procedures failed to start the engine I made an off field landing in a soy bean field. The aircraft struck a ditch and flipped over destroying aircraft.' Reported flight time for the accident flight was three and a half hours. A FAA on-scene examination revealed no anomalies. Approximately one half gallon of fluid was found on the ground around each of the fuel tank's cap vent areas. A Cessna 150 performance-specification page stated, 'RANGE: Cruise, ... 22.5 Gallons, No Reserve ... 4.1 hrs.'
Probable Cause: the improper in-flight decision of the pilot to fly past the Vandalia airport onto Saint Louis Regional and the fuel exhaustion. A factor was the ditch.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI00LA159 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20001212X21179&key=1
History of this aircraft
Other occurrences involving this aircraft Revision history:
Date/time | Contributor | Updates |
27-Jan-2015 19:47 |
harro |
Updated [Operator, Narrative] |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
12-Dec-2017 18:48 |
ASN Update Bot |
Updated [Departure airport, Destination airport, Source, Narrative] |
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