ASN Wikibase Occurrence # 134065
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 12 October 1996 |
Time: | 03:23 LT |
Type: | Piper PA-28-181 |
Owner/operator: | Plus One Flyers |
Registration: | N2501X |
MSN: | 28-8590079 |
Total airframe hrs: | 4733 hours |
Engine model: | Lycoming O-360-A4M |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | San Diego, CA -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Unknown |
Departure airport: | (KMYF) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to information from the flying club that had operational control of the airplane, the airplane was taken without permission by a student pilot, who was a former member of the club. A police report was filed. Later, an investigation revealed that the student had taken the airplane after attending a party where he met his passenger. At about 0045 PDT, the student took off on a night flight. After about 2.7 hours of flight time, the airplane collided with high tension power lines, which were strung diagonally across a major city freeway. The accident site was 1.5 miles from the departure airport, and the power lines were about 75 feet above the pavement. The 0315 PDT weather at the airport was in part: 400 feet overcast, visibility 3 miles with fog, and wind calm. A toxicology test of the pilot's blood (drawn shortly after the accident) showed an alcohol level of 80 mg/dl (0.08%). Witnesses indicated that the pilot had been drinking beer at a party until almost midnight.
Probable Cause: the student pilot's impairment of judgment and performance due to alcohol, his subsequent flight into adverse weather conditions, and his failure to maintain clearance from obstructions (power lines). Factors related to the accident were: darkness, low ceiling, and fog.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX97LA013 |
Status: | Investigation completed |
Duration: | 1 year and 2 months |
Download report: | Final report |
|
Sources:
NTSB LAX97LA013
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
21-Dec-2016 19:26 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
08-Apr-2024 18:33 |
ASN Update Bot |
Updated [Time, Other fatalities, Departure airport, Source, Narrative, Category, Accident report] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation