ASN Wikibase Occurrence # 134255
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 15 July 2001 |
Time: | 19:00 |
Type: | Cessna 175 Skylark |
Owner/operator: | Private |
Registration: | N8861E |
MSN: | 56161 |
Year of manufacture: | 1959 |
Total airframe hrs: | 2755 hours |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Mooresville, NC -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | Moresville, NC (14A) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to the pilot the engine was surging as the airplane started its takeoff roll. When the airplane became airborne the pilot reported he could not maintain altitude and elected to make a forced landing, coming to rest upside down in a tree about 40 feet above the ground. The pilot stated he was flying solo, landed at an airport, and on takeoff "...the engine didn't feel right on full throttle." He and a co-owner of the airplane tried to find the problem, but they could not. They then decided to fly to the airport where the accident eventually took place. They landed twice, and on the second takeoff the pilot stated "...the problem showed up, landing us in the trees." The fuel burn for this airplane was 10 to 10.5 gallons per hour in level flight. Each fuel tank held 26 gallons, for a total of 52 gallons, of which 9 gallons of fuel was unusable, or 43 gallon of usable fuel. The fuel tanks were topped off on June 28, 2001. The owner/student pilot did not log all the time since last refueling the airplane, but 3.98 hours were logged. At 10.5 gallon per hour, 41.79 gallons of fuel would have been used in 3.98 hours. Examination of the fuel system after the accident revealed that about 2 gallons of fuel was drained from the left tank, and no fuel was found in the right tank. The fuel that was drained was clean with no evidence of sediment or water. In addition, there was no evidence of fuel leaks found at the accident site, and no fuel odor was noted at the accident site. Examination of the propeller and engine revealed no discrepancies.
Probable Cause: the pilot's improper fuel consumption calculations, inadequate preflight planning, and failure to refuel the airplane before takeoff, which resulted in a loss of engine power due to fuel exhaustion, and a forced landing in trees.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA01LA185 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20010720X01469&key=1 Location
Revision history:
Date/time | Contributor | Updates |
21-Dec-2016 19:26 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
10-Dec-2017 11:53 |
ASN Update Bot |
Updated [Other fatalities, Departure airport, Source, Narrative] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation