Wirestrike Accident Piper PA-28R-180 N3708T,
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ASN Wikibase Occurrence # 134676
 
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Date:Thursday 31 May 2001
Time:20:34
Type:Silhouette image of generic P28R model; specific model in this crash may look slightly different    
Piper PA-28R-180
Owner/operator:Private
Registration: N3708T
MSN: 28R-30012
Year of manufacture:1967
Total airframe hrs:9500 hours
Engine model:Lycoming IO-360-B1E
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Destroyed
Category:Accident
Location:Albuquerque, NM -   United States of America
Phase: Manoeuvring (airshow, firefighting, ag.ops.)
Nature:Private
Departure airport:Albuquerque, NM (ABQ)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
After taking off and climbing to an altitude of 200 feet, the pilot heard "a single loud pop." The engine continued to develop some power but not enough for the airplane to return to the airport. The pilot said "dusk hampered visibility somewhat," and he didn't see the power lines ahead until it was too late. The right wing struck a power line and was torn off, and the airplane impacted a mesa. Examination disclosed the number 1 (right front, as viewed from the cockpit) cylinder head had separated from the cylinder barrel. The engine had accumulated 1,933.15 hours total time when it was given a "certified overhaul to new engine tolerances zero-time equivalent" and reinstalled in the airplane in 1988. Two years later, all of the cylinders were removed and the camshaft lobes and lifter faces were visually inspected for premature wear and galling. No unusual wear was noted. Only routine maintenance was recorded thereafter. At the time of the accident, the engine had accrued 1,585.04 hours since overhaul.
Probable Cause: the pilot's diminished visual lookout, resulting in the wire strike. Contributing factors were the total mechanical failure of the cylinder, dusk, and the power transmission line.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: DEN01LA107
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20010608X01109&key=1

Revision history:

Date/timeContributorUpdates
21-Dec-2016 19:26 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
10-Dec-2017 11:23 ASN Update Bot Updated [Other fatalities, Departure airport, Source, Narrative]
26-Sep-2018 12:47 BEAVERSPOTTER Updated [Cn]

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