ASN Wikibase Occurrence # 134973
Last updated: 26 May 2013
This information is added by users of ASN. ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can submit corrected information
Narrative:The active duty military pilot rented the airplane, while on leave, for a flight from Honolulu, Hawaii, to the island of Maui, and return. He received a checkout flight (1.2 hours) in the aircraft the day before. The pilot topped off the fuel tanks, which gave him 22.5 gallons useable, before the flight. The flight over was uneventful, but on his return flight, he lost total engine power at 2,000 feet, approximately 10 nautical miles east of his destination. The pilot described the power loss as follows: "The engine smoothly 'rolled back' in RPM to something less than cruise power as if power was simply reduced. It ran smoothly with no inconsistency for approximately one minute, and then completely stopped." He successfully ditched the aircraft into the Pacific Ocean. The two occupants exited the aircraft with an inflatable raft and were rescued.
|Operator:||Georges Aviation Services Inc.|
|C/n / msn:|| 15070008|
|Fatalities:||Fatalities: 0 / Occupants: 2|
|Airplane damage:|| Written off (damaged beyond repair)|
|Location:||Honolulu, HI -
United States of America
|Phase:|| En route|
Air traffic control tower records indicate that the pilot's flight time to Maui was 1 hour, 34 minutes, and his return flight from takeoff to ditching was 45 minutes. The airplane's fuel consumption rate should have been between 6 and 7 gallons per hour. The airplane sank in deep water, and was not recovered.
PROBABLE CAUSE:The total loss of engine power for an undetermined reason. A factor was the lack of suitable terrain for a forced landing.
NTSB id 20070723X00993
Number of views: 226