ASN Wikibase Occurrence # 135270
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Date: | Thursday 15 May 2003 |
Time: | 17:00 |
Type: | Cessna 320D Skyknight |
Owner/operator: | Strata Production Company |
Registration: | N4111T |
MSN: | 320d0011 |
Year of manufacture: | 1965 |
Total airframe hrs: | 3703 hours |
Engine model: | Continental TSIO-520-BB |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | El Paso, TX -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | El Paso International Airport, TX (ELP/KELP) |
Destination airport: | Roswell International Air Center Airport, NM (ROW/KROW) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:While executing a left turn for a crosswind departure, approximately 700-800 feet agl, the 1,104-hour private pilot reported he "lost the left engine," and the pilot attempted to land on the airport taxiway. The airplane impacted the hard surface taxiway in a left wing nose low attitude, came to rest upright, and was partially consumed by a post-impact fire. Prior to departure, the pilot performed an engine run-up and the run-up was normal. One witness reported the takeoff was normal, and the airplane made a left turn for a crosswind departure. During the turn, the left wing came down, then the right, then the left again, and the airplane developed a very high sink rate. Two other witnesses reported the airplane "seemed like it was in trouble...something [was] terribly wrong...the aircraft may have stalled then pitched nose down and then we knew he was coming down." Approximately the time of the accident, the winds were reported 22 knots, gusting to 40 knots, and peak winds from 40 to 44 knots. According to the airplane's performance charts, the calculated airplane's single-engine climb performance was approximately 300 feet per minute. Examination of the airframe and engines did not disclose any structural or mechanical anomalies that would have prevented normal operation. The reason for the reported loss of engine power was not determined.
Probable Cause: the loss of engine power for undetermined reasons and the pilot's failure to maintain aircraft control. Contributing factors were the gusty and high wind conditions, and the pilot's failure to compensate for the wind conditions.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW03LA150 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20030520X00694&key=1 Location
Revision history:
Date/time | Contributor | Updates |
21-Dec-2016 19:26 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
08-Dec-2017 18:45 |
ASN Update Bot |
Updated [Other fatalities, Departure airport, Destination airport, Source, Narrative] |
16-Nov-2022 20:28 |
Ron Averes |
Updated [Aircraft type, Departure airport, Destination airport] |
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