Loss of control Accident Cessna T182T Turbo Skylane N6062E,
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ASN Wikibase Occurrence # 142412
 
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Date:Thursday 9 February 2012
Time:13:45
Type:Silhouette image of generic C182 model; specific model in this crash may look slightly different    
Cessna T182T Turbo Skylane
Owner/operator:Private
Registration: N6062E
MSN: T18208595
Year of manufacture:2006
Total airframe hrs:583 hours
Engine model:Lycoming TIO-540-AK1A
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Lebanon Municipal Airport - KLEB, NH -   United States of America
Phase: Approach
Nature:Private
Departure airport:Lebanon, NH (LEB)
Destination airport:Lebanon, NH (LEB)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
During the takeoff climb from runway 36, when the airplane was about 1/2 mile from the runway and at an altitude of 1,500 feet mean sea level, the pilot told the air traffic controller that he needed to return to land. He did not specify the nature of the problem. The pilot aligned the airplane for landing on runway 18 but was too high and fast to land. The airplane continued beyond the departure end of the runway and appeared to enter a modified downwind and base traffic pattern for runway 36. However, witnesses observed the airplane pass through the final approach and then make a sharp left turn back toward runway 36. During that turn, the airplane appeared to stall and subsequently impacted the grass east of runway 36. The airplane had been in a reasonable position to land on runway 36 before it passed through the final approach.


No preimpact anomalies were noted with the airplane or engine. Examination of the engine revealed that the intake and exhaust springs were shorter than the length prescribed by the manufacturer. If the springs were in this condition before the accident, it is likely the pilot would have noticed some engine roughness. However, it is also possible that the springs may have lost tension during the postcrash fire.

Testing of the fuel that was added to the airplane just before takeoff revealed no anomalies. The airplane had flown 8 hours since its most recent annual inspection, which occurred 3 months before the accident. It was unclear how much recent flight time the pilot had accumulated; his most recent logged experience was 3 months before the accident.
Probable Cause: The pilot’s failure to maintain airspeed during a return to the airport after takeoff, which resulted in an aerodynamic stall and loss of airplane control.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA12FA175
Status: Investigation completed
Duration: 1 year and 6 months
Download report: Final report

Sources:

NTSB

Location

Revision history:

Date/timeContributorUpdates
09-Feb-2012 16:57 Geno Added
09-Feb-2012 17:04 Geno Updated
09-Feb-2012 23:28 RobertMB Updated [Time, Aircraft type, Phase, Source, Narrative]
10-Feb-2012 00:32 Gluchich Updated [Source]
22-Feb-2012 21:42 Geno Updated [Source]
21-Dec-2016 19:26 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
27-Nov-2017 20:19 ASN Update Bot Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative]

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