Fuel exhaustion Accident Beechcraft 77 Skipper N18012,
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ASN Wikibase Occurrence # 146210
 
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Date:Thursday 7 June 2012
Time:16:15
Type:Silhouette image of generic BE77 model; specific model in this crash may look slightly different    
Beechcraft 77 Skipper
Owner/operator:Private
Registration: N18012
MSN: WA-276
Engine model:Lycoming O-235 SERIES
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Clark, SD -   United States of America
Phase: Landing
Nature:Private
Departure airport:Pierre, SD (PIR)
Destination airport:Morris, MN (MOX)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The passenger reported that the airplane’s low fuel light illuminated during the flight. She stated that they continued the flight and were circling to land on a grass runway when the airplane crashed. A witness reported seeing the airplane pass over the runway at a low altitude with the engine operating. The airplane then abruptly climbed and initiated a turn. The witness said that the airplane’s nose dropped as if the airplane had stalled and it then descended and impacted the ground. The airplane incurred substantial damage, which included separation of the engine, outboard left wing and aft fuselage, and upward bending of the right wing. There was no bending of the blades of the engine’s propeller, indicating that the engine was not producing power at the time of the impact. Both fuel tanks ruptured, and only 1 gallon of fuel was recovered at the scene. No fuel was found in the gascolator or carburetor. No fuel odor was present at the accident site. The airplane maintenance manual indicated that 1 gallon of the airplane’s fuel supply was unusable fuel. It is likely that the engine lost power during the landing approach due to fuel exhaustion and that the pilot failed to maintain airspeed after the power loss, resulting in an inadvertent stall.
Probable Cause: The pilot’s improper fuel management, which led to fuel exhaustion, and his failure to maintain adequate airspeed resulting in an aerodynamic stall.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN12LA346
Status: Investigation completed
Duration: 1 year and 3 months
Download report: Final report

Sources:

NTSB

Location

Revision history:

Date/timeContributorUpdates
08-Jun-2012 13:47 Geno Added
08-Jun-2012 15:44 RobertMB Updated [Aircraft type, Source, Narrative]
08-Jun-2012 23:00 Anon. Updated [Aircraft type, Source, Narrative]
21-Dec-2016 19:28 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
27-Nov-2017 20:46 ASN Update Bot Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative]

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