Accident Interplane Skyboy EX N582YB,
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ASN Wikibase Occurrence # 147157
 
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Date:Friday 27 July 2012
Time:18:30
Type:Interplane Skyboy EX
Owner/operator:Private
Registration: N582YB
MSN: 06192001735
Year of manufacture:2001
Total airframe hrs:160 hours
Engine model:Rotax 582
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:SE Oral Hull Road, Sandy, OR -   United States of America
Phase: Landing
Nature:Private
Departure airport:Sandy, OR (03S)
Destination airport:Sandy, OR (03S)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot had been flying the airplane for about 1 hour before the accident. He landed, shut down the engine, boarded new passengers, and restarted the engine. The total time from shut down to start up was about 5 minutes. He stated that the airplane's engine performed normally during run-up and takeoff. After takeoff, about 300 to 400 feet above ground level, the engine began to lose power. The pilot made a hard right turn and landed in an open field. The airplane impacted a fence post with its right wing during the landing roll. An engine examination revealed that the engine did not have a carburetor heat system installed. The subsequent engine test run on the airframe confirmed that a partial loss of engine power occurred after about 1.5 minutes of operation. The temperature, dew point, and relative humidity were nearly identical during the engine test run and the accident event. A carburetor icing chart indicated the possibility of serious carburetor icing at cruise power at the reported atmospheric conditions. The engine was removed from the airframe, examined, and tested at an engine tech services facility. During the engine test run the engine performed at various power levels for 28 minutes without degraded power output. The atmospheric conditions during this test were significantly different than the conditions at the time of the accident. The engine inspection concluded that there were no anomalies that would have precluded normal operation.
Probable Cause: A partial loss of engine power during takeoff due to carburetor icing. Contributing to the accident was the lack of a carburetor heat system installed on the airplane.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR12LA329
Status: Investigation completed
Duration: 1 year and 9 months
Download report: Final report

Sources:

NTSB
FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=582YB

Location

Revision history:

Date/timeContributorUpdates
28-Jul-2012 14:39 Geno Added
28-Jul-2012 14:51 Geno Updated [Aircraft type, Registration, Cn, Source, Narrative]
07-Dec-2012 11:06 Anon. Updated [Source, Narrative]
21-Dec-2016 19:28 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
27-Nov-2017 20:54 ASN Update Bot Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative]

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