ASN Wikibase Occurrence # 147159
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Date: | Friday 27 July 2012 |
Time: | 15:09 |
Type: | Piper PA-24-250 Comanche |
Owner/operator: | Private |
Registration: | N6248P |
MSN: | 24-1355 |
Year of manufacture: | 1959 |
Total airframe hrs: | 6368 hours |
Engine model: | Lycoming O-540 SERIES |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Virginia Tech/Montgomery Executive Airport - KBCB, Blacksburg, VA -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Crestview, FL (CEW) |
Destination airport: | Blacksburg, VA (BCB) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane was approaching the destination airport, and, according to the pilot, the left fuel selector was set to the left main tank and the right fuel selector was set to the right main tank. The engine began to lose power, and the pilot subsequently applied carburetor heat and placed the right fuel selector to the right tip tank position. However, the engine did not regain power. The pilot made a forced landing in the airport parking lot, and the airplane collided with a perimeter fence, resulting in structural wing damage.
Postaccident examination of the wreckage revealed that neither of the main fuel tanks contained usable fuel. The right tip tank contained about 7.5 gallons of fuel; however, the fuel selector was placarded with a note stating that the tip tanks were for use in level flight only. With the left main tank selected and no fuel in that tank, air would have been introduced into the fuel system, resulting in fuel starvation. The pilot’s preflight planning indicated an en route time of 2 hours 32 minutes. However, when the loss of power occurred, the flight had been airborne for about 3 hours 39 minutes. The pilot reported that he was not sure if the airplane’s fuel gauges were accurate, so he relied on fuel burn rate calculations during the flight.
Probable Cause: The pilot’s inadequate preflight planning and improper in-flight fuel management, which resulted in a total loss of engine power due to fuel starvation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA12LA486 |
Status: | Investigation completed |
Duration: | 9 months |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://myfox8.com/2012/07/28/plane-runs-into-fence-at-blacksburg-airport/ http://www.roanoke.com/news/roanoke/wb/312138 http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=6248P https://flightaware.com/live/flight/N6248P http://myfox8.com/2012/07/28/plane-runs-into-fence-at-blacksburg-airport/ http://www.roanoke.com/news/roanoke/wb/312138 http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=6248P https://flightaware.com/live/flight/N6248P Location
Revision history:
Date/time | Contributor | Updates |
28-Jul-2012 17:48 |
Geno |
Added |
29-Jul-2012 00:27 |
Alpine Flight |
Updated [Nature, Damage, Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
27-Nov-2017 20:53 |
ASN Update Bot |
Updated [Operator, Total occupants, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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