ASN Wikibase Occurrence # 149130
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Date: | Thursday 13 September 2012 |
Time: | 13:20 |
Type: | Best Off Skyranger |
Owner/operator: | Private |
Registration: | N936LS |
MSN: | SKR0306325 |
Year of manufacture: | 2004 |
Total airframe hrs: | 1066 hours |
Engine model: | Rotax 912UL |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Near Lake Matthews, four miles west of Perris, CA -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Corona, CA (AJO) |
Destination airport: | Perris, CA (L65) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During cruise flight in the experimental amateur-built airplane, the pilot heard a "bang" sound, and the airplane immediately began to descend and roll to the left. He applied opposing aileron and right rudder control inputs and was able to regain partial control; however, as the descent progressed, the airplane's turn rate began to increase. The airplane struck the ground in a left-wing-low attitude, sustaining substantial damage. Examination of the airframe did not reveal any failures or anomalies that would have precluded normal operation.
Although postaccident examination of the wreckage revealed two separated cables (a wing brace and an elevator trim tab cable), physical evidence indicated that the cable separations most likely occurred during the accident sequence. Additionally, if the elevator trim tab cable had separated in flight, the movement of the trim tab to the up position likely would not have resulted in the flight control difficulties experienced by the pilot. Thus, it was not possible to determine why the airplane departed controlled flight and why the pilot was unable to regain control.
Probable Cause: A loss of aircraft control during cruise flight for reasons that could not be determined because postaccident examination did not reveal any anomalies that would have precluded normal operation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR12LA417 |
Status: | Investigation completed |
Duration: | 1 year and 4 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
14-Sep-2012 02:21 |
gerard57 |
Added |
14-Sep-2012 09:16 |
Geno |
Updated [Time, Aircraft type, Registration, Cn, Location, Source, Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
28-Nov-2017 13:24 |
ASN Update Bot |
Updated [Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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