ASN Wikibase Occurrence # 149350
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Date: | Sunday 30 September 2012 |
Time: | 16:30 |
Type: | Air Creation Tanarg |
Owner/operator: | Private |
Registration: | N2751N |
MSN: | T05004 |
Engine model: | Rotax 912 UL |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Near San Carlos on the White Mountain Indiana Reservation, AZ -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Safford, AZ (SAD) |
Destination airport: | Show Low, AZ (SOW) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:While flying in loose formation with another airplane to the destination airport, the accident airplane descended to about 400 feet above ground level. The pilot subsequently advised the pilot of the other airplane that the wind had become stronger and was affecting his airplane’s controllability. He added that he might attempt to land or consider returning to the departure airport. Shortly thereafter, the airplane made a descending right turn and impacted the ground.
An examination of the wreckage revealed that the airplane was equipped with a nonstandard, smaller wing and was trimmed to the near full nose-down position, which would increase the airplane’s stall speed. According to the wing manufacturer, the nonstandard wing has controllability problems at high speeds. Surface weather observations reported wind gusting to 22 knots near the time of the accident. The combination of the nonstandard wing, which reduced controllability, the full nose-down trim, which increased the stall speed, and the high wind gusts resulted in the pilot’s failure to maintain control of the airplane.
Postmortem toxicological testing of specimens from the pilot indicated the recent use of marijuana. Although the levels were such that the use may have been impairing, the actual effects on the flight could not be determined.
Probable Cause: The pilot’s failure to maintain airplane control while maneuvering in high wind conditions and his failure to adjust the trim appropriately. Contributing to the accident was the airplane’s nonstandard modified wing configuration.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR12LA442 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
30-Sep-2012 23:51 |
gerard57 |
Added |
08-Oct-2012 11:27 |
harro |
Updated [Aircraft type, Registration, Cn, Location, Source] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
28-Nov-2017 13:27 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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