ASN Wikibase Occurrence # 149422
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Thursday 4 October 2012 |
Time: | 09:30 |
Type: | Bushby Mustang II FB |
Owner/operator: | Private |
Registration: | N112MW |
MSN: | 963 |
Total airframe hrs: | 1 hours |
Engine model: | Lycoming IO-360-A1A |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Near San Manuel Airport in Pinal County -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | San Manuel, AZ (E77) |
Destination airport: | San Manuel, AZ (E77) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was flying on the first flight in the airplane since certification. Shortly after takeoff, he reported over a common airport frequency that the airplane had low engine oil pressure and that he was returning to the airport to land. Witnesses observed the airplane maneuver from the downwind leg to final approach for the intended runway by executing a 180-degree left turn. One witness observed the airplane's bank increase to about 90 degrees and descend out of sight. Another witness observed that the airplane was low and slow and appeared to stall. The witness stated that the left wing dropped and that the airplane went straight down.
Postaccident examination of the airframe, flight control components, and the engine revealed no evidence of mechanical malfunctions or failures that would have precluded normal operation. It is likely that, because this was the pilot's first flight in the airplane and he was distracted by the low oil pressure, he failed to maintain adequate airspeed while maneuvering, and the airplane subsequently stalled. The toxicology report indicated that the pilot was taking medication for several medical conditions; however, insufficient information was available to determine if the pilot's medical conditions contributed to the accident.
Probable Cause: The pilot's failure to maintain adequate airspeed while maneuvering to final approach due to his distraction by the low engine oil pressure, which resulted in an aerodynamic stall.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR13LA002 |
Status: | Investigation completed |
Duration: | 1 year and 8 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
05-Oct-2012 00:00 |
gerard57 |
Added |
05-Oct-2012 11:45 |
RobertMB |
Updated [Aircraft type, Registration, Cn, Source] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
28-Nov-2017 13:45 |
ASN Update Bot |
Updated [Other fatalities, Departure airport, Destination airport, Source, Narrative] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation