Accident Piper PA-30 Twin Comanche N7017Y,
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ASN Wikibase Occurrence # 156857
 
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Date:Thursday 20 June 2013
Time:09:30
Type:Silhouette image of generic PA30 model; specific model in this crash may look slightly different    
Piper PA-30 Twin Comanche
Owner/operator:Horizon Aviation LLC
Registration: N7017Y
MSN: 30-18
Year of manufacture:1963
Total airframe hrs:4254 hours
Engine model:Lycoming IO-320 SERIES
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:James M Cox Dayton International Airport, Dayton, Ohio -   United States of America
Phase: Take off
Nature:Private
Departure airport:Dayton, OH (KDAY)
Destination airport:Urbana, OH (I74)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot stated that, during the preflight inspection of the airplane, he found a small amount of water in the right inboard fuel tank. The pilot inspected the other fuel tanks and did not find any water; he then rechecked the right inboard fuel tank and did not find any additional water. During startup, the right engine stopped, but the pilot restarted it and ran it with a higher rpm during warm-up. The pilot stated that the taxi and run-up were performed without hesitation or problems but that the takeoff run seemed “sluggish” and that the airplane then drifted right. The pilot was unable to correct the drift by applying rudder, so he reduced the throttles and chose to perform a force landing on a closed taxiway. The airplane landed short of the taxiway and impacted a bump in the terrain, which caused the landing gear to collapse. Although water in the right engine’s fuel tank could have resulted in power loss and the subsequent drift to the right, examination of the airplane did not find any water in the fuel nor any abnormalities that would have prevented the engines from producing power. A reason for the pilot’s loss of directional control could not be determined.

Probable Cause: The pilot’s loss of control of the airplane for reasons that could not be undetermined because a postaccident examination of the airplane did not reveal any anomalies that would have precluded normal operation.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN13LA361
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB
FAA register: 2. FAA: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=7017Y

4. https://flightaware.com/resources/registration/N7017Y

Location

Revision history:

Date/timeContributorUpdates
20-Jun-2013 11:30 gerard57 Added
20-Jun-2013 16:40 Geno Updated [Time, Registration, Cn, Operator, Location, Destination airport, Source]
21-Jun-2013 02:04 BTD1 Updated [[Time, Registration, Cn, Operator, Location, Destination airport, Source]]
21-Jun-2013 03:39 Alpine Flight Updated [Aircraft type, Departure airport, Damage, Narrative]
21-Jun-2013 06:04 harro Updated [Time, Phase, Narrative]
21-Dec-2016 19:28 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
16-Apr-2017 17:13 Dr.John Smith Updated [Time, Location, Departure airport, Destination airport, Source, Narrative]
29-Nov-2017 08:45 ASN Update Bot Updated [Time, Other fatalities, Departure airport, Destination airport, Source, Narrative]

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