ASN Wikibase Occurrence # 157350
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Date: | Saturday 29 June 2013 |
Time: | 12:10 |
Type: | Less Drag Special |
Owner/operator: | Private |
Registration: | N130LD |
MSN: | 1 |
Year of manufacture: | 2010 |
Total airframe hrs: | 140 hours |
Engine model: | Lycoming IO-540-D4B5 |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Field near Oxnard Airport (KOXR), Oxnard, CA -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Oxnard, CA (OXR) |
Destination airport: | Oxnard, CA (OXR) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Two witnesses stated that they observed the airplane taxi out and take off, and they reported that the engine sounded good. Additional witnesses reported seeing the airplane depart and then hearing the engine backfire and sputter before losing power. The airplane banked left as if the pilot were trying to return to the airport. The airplane’s nose pitched up, it stalled, and then its nose pitched down before it impacted terrain. A postimpact fire destroyed the fuselage, cabin, cockpit, and right wing. The left wing and empennage were seriously damaged by the fire and impact forces. No anomalies were noted during the postaccident examination that would have resulted in the loss of engine power or the subsequent loss of airplane control. The witnesses' descriptions of the event were consistent with the airplane entering an aerodynamic stall/spin while the pilot was attempting to return to the airport after encountering a loss of engine power during initial climb. A review of weight and balance data revealed that the airplane would have been within its center of gravity limits at the time of the accident.
Probable Cause: A loss of engine power after takeoff for reasons that could not be determined because postaccident examination did not reveal any anomalies that would have precluded normal operation, and the pilot’s failure to maintain adequate airspeed, which resulted in an aerodynamic stall/spin.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR13FA298 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
30-Jun-2013 02:01 |
Geno |
Added |
30-Jun-2013 12:32 |
snj |
Updated [Source] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
29-Nov-2017 08:44 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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