Accident Beechcraft A36 Bonanza N40KG,
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ASN Wikibase Occurrence # 160860
 
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Date:Monday 23 September 2013
Time:12:37
Type:Silhouette image of generic BE36 model; specific model in this crash may look slightly different    
Beechcraft A36 Bonanza
Owner/operator:Fourstars Aviation
Registration: N40KG
MSN: E-1283
Year of manufacture:1978
Engine model:Teledyne Continental IO-550-B
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:NW of Boca Raton, FL -   United States of America
Phase: En route
Nature:Private
Departure airport:Herndon, VA (IAD)
Destination airport:Boca Raton, FL (BCT)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot departed for a planned 4-hour instrument flight rules, cross-country flight, and about 5 hours 13 minutes into the flight, the engine lost power. The pilot reported that he then landed the airplane on a wet roadway and lost directional control as the wheels hydroplaned on the wet surface. The airplane subsequently struck a sign and electrical power pole, resulting in substantial damage. The quantity of fuel onboard the airplane at the time of the accident could not be determined due to damage sustained to the airframe during the accident. Although the pilot advised an air traffic controller during the forced landing, “I believe I ran out of fuel,” at least 12 usable gallons should have remained based on the amount of fuel the pilot reported the airplane had before departing on the flight and the total fuel use calculated by an onboard fuel flow indicator.
A postaccident test run of the engine showed that it started normally and ran with no anomalies noted. Download of non-volatile memory from an engine monitoring device showed that the loss of engine power was immediately preceded by a rise in exhaust gas temperature and a rapid reduction in fuel flow, consistent with an interruption of fuel flow. The pilot did not report the position of the fuel selector before the loss of engine power, and its preaccident position could not be determined because the pilot had selected it to the off position before egressing the airplane after the accident.

Probable Cause: A total loss of engine power due to an interruption in fuel flow, which was most likely due to fuel starvation. Contributing to the accident was the pilot’s failure to maintain control of the airplane while performing the subsequent forced landing to a wet roadway.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA13LA428
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB
https://flightaware.com/live/flight/N40KG/history/20130923/1000Z/KIAD/KBCT

Location

Media:

Revision history:

Date/timeContributorUpdates
23-Sep-2013 17:58 harro Added
21-Dec-2016 19:28 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
29-Nov-2017 09:15 ASN Update Bot Updated [Total occupants, Other fatalities, Nature, Departure airport, Destination airport, Source, Embed code, Narrative]

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