ASN Wikibase Occurrence # 161677
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Date: | Friday 25 October 2013 |
Time: | 11:45 |
Type: | Cessna 172M Skyhawk |
Owner/operator: | Private |
Registration: | N20587 |
MSN: | 17261419 |
Year of manufacture: | 1973 |
Engine model: | Lycoming 0-320 SERIES |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Near Bell Airfield (XS56), Raymondville, TX -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Rio Grande City, TX (67R) |
Destination airport: | Raymondville, TX (XS56) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The non-certificated pilot said he flew his unregistered airplane for about 2 hours "recreationally" before attempting to land at a privately owned airport, where he said the airplane was scheduled to have an annual inspection completed. The pilot said a gust of wind blew the airplane off course while on final approach and he attempted to go-around. The airplane then stalled and impacted a field short of the runway, which resulted in substantial damage to the firewall and empennage. Though the pilot did not report an engine failure, examination of the airplane revealed both fuel tanks were empty and damage to the propeller was consistent with it not turning at the time of impact. The pilot reported there were no mechanical deficiencies that would have precluded normal operation of the airplane and engine. The pilot did not have a valid Federal Aviation Administration (FAA) medical and had a reported history of a stroke. The pilot's daughter also reported that her father was starting to show symptoms of Sundowner's Syndrome.
Probable Cause: The operation of an airplane by a non-certificated pilot. Contributing to the accident was his failure to maintain airspeed following a total loss of engine power at low altitude, which resulted in an aerodynamic stall. Also contributing was the pilot's improper fuel management, which resulted in a total loss of engine power due to fuel exhaustion.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN14CA027 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=20587 Location
Revision history:
Date/time | Contributor | Updates |
25-Oct-2013 19:20 |
Geno |
Added |
25-Oct-2013 21:43 |
Geno |
Updated [Time, Aircraft type, Registration, Cn, Operator, Phase, Destination airport, Source, Damage, Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
29-Nov-2017 09:18 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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