ASN Wikibase Occurrence # 162624
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Date: | Wednesday 4 December 2013 |
Time: | 12:25 |
Type: | Bellanca 7GCBC |
Owner/operator: | Private |
Registration: | N88342 |
MSN: | 768-74 |
Year of manufacture: | 1974 |
Total airframe hrs: | 1848 hours |
Engine model: | Lycoming O-320-A2D |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Dutch Landing Strip (88AK), Sterling, AK -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Sterling, AK |
Destination airport: | Port Graham, AK (PGM) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The uncertificated student pilot stated that he had been watching the weather for three days waiting for suitable flying conditions. He checked the automated weather at a nearby airport, and decided that conditions were suitable for flying. He and a passenger then took off on a cross-country flight. During the climb to cruise altitude, the uncertificated student pilot began to notice specks of ice on the windscreen. A short time later, ice suddenly began to accumulate rapidly on the airplane, obscuring the windscreen. He could see an airstrip ahead and to the left of the airplane, and started a rapid descent to set up for a landing. As he approached the airstrip, he said that he was still too fast and too high to attempt a landing, so he initiated a go-around. During the second landing attempt, he said that the airplane felt very heavy and sluggish, and as he began to slowly decrease the throttle on the landing approach, the airplane began to lose altitude very fast. He attempted a second go-around, but the engine backfired and lost power. He landed the airplane just past the end of the airstrip on a dirt road, but the right wing struck a power line guy wire, and the airplane spun to the right, striking a road sign. The airplane sustained substantial damage to the right wing and empennage. The pilot stated that there were no preaccident mechanical anomalies with the airplane that would have precluded normal operation.
Probable Cause: The operation of the airplane by the uncertificated student pilot, his failure to recognize conditions conducive to structural icing, and subsequent decision to depart in conditions conducive to structural icing, resulting in a severe icing encounter and forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ANC14CA010 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=88342 Location
Revision history:
Date/time | Contributor | Updates |
05-Dec-2013 23:23 |
Geno |
Added |
31-Jul-2014 10:23 |
Anon. |
Updated [Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
29-Nov-2017 09:28 |
ASN Update Bot |
Updated [Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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