ASN Wikibase Occurrence # 166810
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Date: | Sunday 8 June 2014 |
Time: | 11:30 |
Type: | Powell P-70 Acey Deucy |
Owner/operator: | Private |
Registration: | N567CM |
MSN: | 045 |
Year of manufacture: | 1997 |
Total airframe hrs: | 492 hours |
Engine model: | Lycoming O-290G |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | North of Great Bend Municipal Airport (KGBD), Great Bend, KS -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Great Bend, KS |
Destination airport: | Great Bend, KS |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The private pilot was conducting a local personal flight. An employee of the fixed-based operator reported that, before takeoff, the pilot topped off the airplane's 18-gallon fuel tank. A witness reported hearing the airplane approach his residence from the north about 2 hours later. The witness said he saw the airplane come out of a cloud bank and that it looked like it was trying to climb at a 45-degree angle. He subsequently saw it in a 45-degree, nose-down pitch angle descending toward the ground. The airplane impacted in a corn field located 6 miles north of pilot's home airport. The witness said the engine sounded "weak as if it had no power" and that, as the airplane was descending, the pilot "was trying to pull up."
An examination of the airplane at the accident site showed that the airplane impacted the ground in a nose-down, steep descent. Flight control continuity was confirmed. Both of the propeller blades were broken at the hub and showed no signs of driving power. An examination of the engine revealed no anomalies that would have prevented it from producing power.
The airplane's fuel tank could hold 18.06 gallons of fuel. The engine manufacturer estimated that the engine's fuel consumption rate at a normal power setting was between 10.5 and 11 gallons per hour; therefore, the airplane would have been able to fly for 1 hour 42 minutes. It is likely that the pilot did not properly plan for the flight, which was longer than allowed by the airplane's total fuel quantity and resulted in loss of engine power due to fuel exhaustion. During the subsequent forced landing to the field, the pilot lost airplane control.
Probable Cause: The pilot's improper preflight planning, which led to a loss of engine power due to fuel exhaustion. Contributing to the accident was the pilot's loss of airplane control during the forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN14FA288 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=567CM Location
Media:
Revision history:
Date/time | Contributor | Updates |
08-Jun-2014 18:19 |
gerard57 |
Added |
08-Jun-2014 18:20 |
harro |
Updated [Aircraft type, Total fatalities, Total occupants, Location, Embed code, Narrative] |
08-Jun-2014 19:05 |
gerard57 |
Updated [Total fatalities, Total occupants, Source, Embed code, Narrative] |
08-Jun-2014 19:07 |
harro |
Updated [Aircraft type, Narrative] |
08-Jun-2014 20:27 |
harro |
Updated [Aircraft type, Registration, Cn, Operator, Embed code, Narrative] |
09-Jun-2014 00:22 |
Geno |
Updated [Time, Operator, Location, Source, Embed code, Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
29-Nov-2017 15:01 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Embed code, Narrative] |
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