ASN Wikibase Occurrence # 167860
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Date: | Thursday 10 July 2014 |
Time: | 11:50 |
Type: | Beechcraft C24R Sierra |
Owner/operator: | Southeast Aviation Services, Inc. |
Registration: | N6222Q |
MSN: | MC-771 |
Year of manufacture: | 1982 |
Total airframe hrs: | 2835 hours |
Engine model: | Lycoming IO-360-A1B6 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | SW of Arthur Dunn Air Park (X21), Titusville, FL -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Titusville, FL (TIX) |
Destination airport: | Titusville, FL (TIX) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that, while conducting a preflight inspection, he looked inside the wing fuel tanks and estimated that there was about 27 gallons of fuel. He then departed on a local flight to test the avionics and autopilot system. While returning to the airport after an approximate 1-hour flight, the engine experienced a total loss of power, and the pilot attempted a forced landing on the roof of a building. The airplane crashed through the roof, which resulted in substantial damage to the wings, fuselage, and flight control surfaces.
No visible fuel or fuel odor was noted at the accident site. A postaccident examination of the airplane revealed that both fuel tanks had been breached and were void of fuel. The fuel strainer sump, which sits forward of the firewall below the fuselage, was found in the open-and-locked position. When the strainer valve’s tangs were pushed up and rotated counter-clockwise, the sump remained in the open-and-locked position. The sump sprang back to the closed position when the tangs were pushed up and released. Postaccident fuel consumption calculations and fuel strainer drain testing revealed that the airplane would have burned through and lost about 28 gallons of fuel during the approximate 1-hour flight with the strainer drain not properly secured.
Probable Cause: The pilot's failure to secure the fuel strainer drain during the preflight inspection, which resulted in a total loss of engine power due to fuel exhaustion.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA14LA336 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
https://flightaware.com/resources/registration/N6222Q Location
Revision history:
Date/time | Contributor | Updates |
10-Jul-2014 18:35 |
Anon. |
Added |
10-Jul-2014 18:37 |
harro |
Updated [Aircraft type, Cn, Operator, Location, Narrative] |
10-Jul-2014 23:56 |
Geno |
Updated [Time, Other fatalities, Location, Departure airport, Source, Narrative] |
31-Jul-2014 04:43 |
Geno |
Updated [Nature, Destination airport, Source, Narrative] |
25-Aug-2014 21:09 |
Aerossurance |
Updated [Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
30-Nov-2017 18:50 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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