Accident Stampe SV.4C G-BPLM,
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ASN Wikibase Occurrence # 167952
 
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Date:Sunday 22 June 2014
Time:17:40 LT
Type:Silhouette image of generic SV4 model; specific model in this crash may look slightly different    
Stampe SV.4C
Owner/operator:Private
Registration: G-BPLM
MSN: 1004
Year of manufacture:1948
Engine model:De Havilland Gipsy Major 10 MK.2
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:½ nm north-west of Paddock Wood, Tunbridge Wells, Kent, England -   United Kingdom
Phase: En route
Nature:Private
Departure airport:Clutton Hill, Somerset
Destination airport:Maidstone-Lashenden (Headcorn) Airfield (EGKH)
Investigating agency: AAIB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
On passing Redhill, during a flight from Clutton Hill in Somerset to Headcorn in Kent, the pilot checked he had sufficient fuel for the remaining 25 nm of the flight. Just west of Paddock Wood, at 1,700 ft amsl, the aircraft was caught in a “particularly harsh” thermal, shortly after which the engine “coughed”.

The pilot considered this to be so unusual that he decided to land immediately at Old Hay Airfield, 1 nm east of Paddock Wood; however, the engine then stopped. He checked the mixture, fuel and magnetos and set up for a forced landing in what looked like a hay field. At about 100 ft, positioned to land a third of the way into the field, the pilot realized the crop was rapeseed which he knew was much denser than hay.

To try to reduce his forward speed on touchdown, he “deep stalled” the aircraft just above the crop; however, the undercarriage caught in the rapeseed and the aircraft slowly pitched over onto its back. With the magnetos and fuel off, he released his full harness and additional lap strap before vacating the aircraft unhurt. The pilot suspected that the problem was caused by the carburettor’s float needle jamming in its base – a problem he was aware had occurred on another Stampe at Headcorn in 2013.

Accident investigation:
cover
  
Investigating agency: AAIB
Report number: EW/G2014/06/38
Status: Investigation completed
Duration:
Download report: Final report

Sources:

1. AAIB: https://assets.digital.cabinet-office.gov.uk/media/548b1252ed915d4c0d0002ae/Stampe_SV4C__Modified__Stampe_G-BPLM_12-14.pdf
2. CAA: http://www.caa.co.uk/aircraft-registration/
3. http://www.bea.aero/fr/enquetes/2014/2014.semaine.28.pdf

Revision history:

Date/timeContributorUpdates
17-Jul-2014 09:21 harro Added
30-Jul-2014 11:38 Alpine Flight Updated [Time, Aircraft type]
13-Dec-2014 10:24 Dr. John Smith Updated [Registration, Cn, Operator, Location, Phase, Nature, Departure airport, Destination airport, Source, Embed code, Narrative]
30-Sep-2015 20:34 Dr. John Smith Updated [Destination airport, Source, Embed code]
29-Jun-2020 05:15 harro Updated [Destination airport, Accident report, ]
26-Jun-2023 09:24 Nepa Updated [[Destination airport, Accident report, ]]

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