ASN Wikibase Occurrence # 168123
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Date: | Friday 11 July 2014 |
Time: | 19:15 |
Type: | Piper PA-18-150 Super Cub |
Owner/operator: | Private |
Registration: | N91106 |
MSN: | 18-8109069 |
Year of manufacture: | 1981 |
Total airframe hrs: | 2477 hours |
Engine model: | Lycoming O-320-A2B |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Van Treese Airport (0CO9), Monte Vista, CO -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Pagosa Springs, CO (PSO) |
Destination airport: | Monte Vista, CO (0CO9) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The private pilot was conducting a personal flight and attempting to land the airplane. He reported that, due to equipment obstructing the 2,600ftlong dirt runway at midfield, he conducted a shallow approach to land on the eastern half of the shortened runway with the airplane pointed west almost directly into the setting sun, which resulted in sun glare. When the airplane was about 100 ft east of the end of the runway, the main landing gear impacted a 2fttall barley crop, which slowed the airplane. The pilot initiated a go-around, but he did not attain sufficient speed to maintain flight and exceeded the airplane’s critical angle-of-attack. The airplane subsequently stalled, impacted terrain on the edge of the runway, and then came to rest inverted, which resulted in substantial damage to both wings, the fuselage, and the vertical tail surfaces. The pilot was not injured and exited the airplane without assistance. The pilot reported that there were no preaccident mechanical deficiencies with the airplane or engine that would have precluded normal operation.
Probable Cause: The pilot’s failure to maintain adequate airspeed and his exceedance of the airplane’s critical angleofattack during a go-around following impact with a barley crop, which resulted in an aerodynamic stall. Contributing to the accident was the pilot’s decision to conduct a shallow approach with the airplane facing directly into the setting sun, which resulted in sun glare.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN14LA361 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=N91106 Location
Revision history:
Date/time | Contributor | Updates |
29-Jul-2014 19:05 |
Geno |
Added |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
30-Nov-2017 18:53 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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