ASN Wikibase Occurrence # 168911
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Date: | Tuesday 19 August 2014 |
Time: | 17:00 |
Type: | Sky Raider |
Owner/operator: | Private |
Registration: | N65692 |
MSN: | 146 |
Year of manufacture: | 2001 |
Total airframe hrs: | 85 hours |
Engine model: | Rotax 447 SCDI |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Farm field west of Hamersville, Ohio -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Hamersville, OH (PVT) |
Destination airport: | Hamersville, OH (PVT) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot departed from a private airstrip that was located on a farm and was bordered by 50-foot-tall trees. He stated that the engine lost power during the initial climb and before the airplane had sufficient altitude to clear the tree line. In an attempt to avoid the trees, the pilot initiated a left turn with the intention of landing in the farm field. The pilot did not recall any further events related to the accident. The airplane’s damage was consistent with a nose-low attitude at impact resulting from an aerodynamic stall while maneuvering after a loss of engine power. A postaccident airframe examination did not reveal any anomalies consistent with a preimpact failure or malfunction. An engine examination revealed that the carburetor had separated from the engine, and the carburetor fuel bowl had separated from the carburetor housing. The carburetor fuel bowl retaining spring clip was dislodged from one of the housing casting holes. Because the carburetor was separated from the engine and the retaining clip was dislodged from the housing casting holes, the investigation was unable to determine whether the carburetor bowl retaining clip was fully engaged before impact. No other anomalies were identified with respect to the engine.
Probable Cause: The pilot's inadvertent aerodynamic stall while maneuvering after a loss of engine power during initial climb. Contributing to the accident was the total loss of engine power for reasons that could not be determined because the investigation could not determine during postaccident examination whether any anomalies existed prior to the accident.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN14LA445 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=65692 Location
Revision history:
Date/time | Contributor | Updates |
20-Aug-2014 04:11 |
Geno |
Added |
06-May-2015 07:11 |
rafranke |
Updated [Phase, Destination airport, Damage, Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
30-Nov-2017 18:59 |
ASN Update Bot |
Updated [Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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