Fuel exhaustion Accident Van's RV-6A N419B,
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ASN Wikibase Occurrence # 169464
 
This record has been locked for editing.

Date:Monday 1 September 2014
Time:17:40
Type:Silhouette image of generic RV6 model; specific model in this crash may look slightly different    
Van's RV-6A
Owner/operator:Private
Registration: N419B
MSN: 21550
Year of manufacture:2001
Total airframe hrs:377 hours
Engine model:Lycoming O-360-C1G
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Marshalltown Municipal Airport (KMIW), Marshalltown, IA -   United States of America
Phase: Landing
Nature:Private
Departure airport:Tea, SD (Y14)
Destination airport:Marshalltown, IA (KMIW)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot said he visually checked and verified that the right wing fuel tank was just under half full and that the left wing fuel tank was just over half full prior to takeoff. As the airplane approached the destination, about 190 nm from the departure airport, the pilot decided to conduct a practice visual approach. Shortly after turning onto final approach, the engine lost power. After employing emergency procedures, the pilot was able to restore power and climbed the airplane to 3,100 feet. He then checked the fuel gauges, which both indicated one-eighth full. The engine then lost power a second time. The pilot made a forced landing in a bean field, and the airplane nosed over. During postaccident examination, no fuel sloshing could be heard when the wings were rocked; both wing fuel caps were then removed from the inverted airplane and no fuel leaked out. The airplane was righted, and when the master switch was turned on, the left fuel gauge was one needle-width above empty and the right fuel gauge indicated empty. The integrity of the fuel tanks appeared to be intact, and no fuel leaked from the tanks. No fuel was visible in either fuel tank. No fuel was recovered when the left and right wing fuel sump drains were removed. After adding fuel, the engine was started and ran at idle power until it was shut down.
Probable Cause: A loss of engine power due to fuel exhaustion as a result of the pilot's misjudgment of the amount of fuel onboard prior to flight.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN14LA472
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB
FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=419B

History of this aircraft

Other occurrences involving this aircraft
1 March 2016 N419B Private 2 near Elmdale Airpark (82TS), Abilene, TX w/o
Loss of control

Location

Revision history:

Date/timeContributorUpdates
02-Sep-2014 16:06 gerard57 Added
03-Sep-2014 02:32 Geno Updated [Time, Aircraft type, Registration, Cn, Location, Departure airport, Destination airport, Source, Damage]
25-Jun-2016 20:23 junior sjc Updated [Aircraft type]
08-Aug-2016 06:15 junior sjc Updated [Narrative]
21-Dec-2016 19:28 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
21-May-2017 06:04 junior sjc Updated [Location, Nature, Departure airport, Destination airport, Source, Narrative]
30-Nov-2017 19:12 ASN Update Bot Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative]

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