ASN Wikibase Occurrence # 170037
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Date: | Saturday 20 September 2014 |
Time: | 15:30 |
Type: | American Champion 7GCBC Citabria Explorer |
Owner/operator: | Rainier Flight Services |
Registration: | N817DH |
MSN: | 1341-2003 |
Year of manufacture: | 2003 |
Total airframe hrs: | 365 hours |
Engine model: | Lycoming O-360 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Tieton State Airport (4S6), Rimrock, Washington -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Rimrock, WA (4S6) |
Destination airport: | Renton, WA (KRNT) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot and pilot-rated passenger of the tailwheel equipped airplane planned to stop at three back country strips before returning to their base airport. The pilot opted not to land at either of the first two planned stops, because she was uncomfortable with the winds at the time of her arrival at each. The third intended destination airport was situated at the shore of a lake. The turf runway was oriented approximately perpendicular to the shoreline, terminated at the shoreline, and was sloped uphill away from the lake. Tall trees and rapidly rising terrain at the other end of the runway resulted in the runway being effectively one way in and one way out, over the lake. The winds were light and variable, and the pilot landed uneventfully at that airstrip. She taxied to the far end, turned around, and began the takeoff roll downhill, towards the lake. She brought the tail up, continued the takeoff roll, and the airplane became prematurely airborne after "rolling over one of the bumpy spots" on the runway. The pilot reported that she tried to fly in ground effect to build airspeed, but lowered the nose too far. The propeller struck the runway, which degraded the airplane performance, and prevented the airplane from successfully climbing. The pilot determined that at that point, she was too far down the runway to safely abort the takeoff on the remaining runway, so she sought a spot straight ahead on the exposed lakebed on which to land the airplane. The pilot steered the airplane towards what appeared to be a dry area that was clear of debris. The airplane struck the dry upslope on the main wheels, and the left main gear impacted a tree stump. The airplane then nosed over to the inverted position. The airplane sustained substantial damage to the wings and fuselage. The pilot reported no preimpact mechanical malfunctions or failures with the airplane that would have precluded normal operation.
Probable Cause: The pilot's failure to maintain aircraft control during takeoff from a rough runway surface which resulted in an off-airport forced landing just beyond the runway.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR14CA383 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
https://flightaware.com/resources/registration/N817DH Location
Revision history:
Date/time | Contributor | Updates |
21-Sep-2014 16:10 |
Geno |
Added |
21-Sep-2014 17:19 |
gerard57 |
Updated [Date] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
30-Nov-2017 19:12 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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