ASN Wikibase Occurrence # 170333
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Date: | Saturday 4 October 2014 |
Time: | 13:43 |
Type: | Rockwell Aero Commander 690B |
Owner/operator: | Rodgers Helicopters / U.S. Forest Service |
Registration: | N700PQ |
MSN: | 11389 |
Year of manufacture: | 1977 |
Total airframe hrs: | 8625 hours |
Engine model: | Garrett TPE-331-5-251 |
Fatalities: | Fatalities: 0 / Occupants: |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Nevada County Airport, CA -
United States of America
|
Phase: | Landing |
Nature: | Fire fighting |
Departure airport: | |
Destination airport: | Nevada County Airport, CA |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Runway excursion / MLG collapse. No injuries reported.
The airline transport pilot reported that, after returning from a fire mission, the airplane floated over the runway and landed long (about 1,500 to 1,800 ft down the runway, which left a maximum of about 2,850 ft of runway remaining). He reduced the power setting to flight idle and then adjusted the thrust levers to (beta) reverse. As the landing roll continued, the pilot adjusted the levers for less reverse thrust. Aware that the ground speed was too fast to make the normal exit turnoff, he applied full reverse thrust again. The airplane then swerved left, departed the runway, impacted some boulders, and came to rest upright in a drainage area.
A postaccident examination of the brake system and engines revealed no evidence of mechanical failures or malfunctions that would have precluded normal operation. If the pilot had initiated a go-around when he realized the airplane was going to land long, he would not have had to modulate the reverse thrust multiple times to make the turnoff.
The National Transportation Safety Board determines the probable cause(s) of this accident as follows:
The pilot’s unstabilized approach and failure to go around and his subsequent failure to maintain directional control during the landing roll.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR15TA002 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
https://www.theunion.com/news/local-news/forest-service-spotter-plane-goes-off-edge-of-airport-runway/ http://fireaviation.com/2014/10/06/air-attack-plane-goes-off-the-runway-at-grass-valley-ca/ http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=700PQ NTSB
Location
Revision history:
Date/time | Contributor | Updates |
07-Oct-2014 10:54 |
Aerossurance |
Added |
07-Oct-2014 18:28 |
gerard57 |
Updated [Total fatalities, Other fatalities, Plane category] |
17-Dec-2016 14:11 |
Aerossurance |
Updated [Time, Operator, Source, Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
12-Nov-2022 01:34 |
Ron Averes |
Updated [Operator, Source] |
24-Sep-2023 05:41 |
Ron Averes |
Updated [[Operator, Source]] |
14-Nov-2023 03:57 |
Ron Averes |
Updated [Operator] |
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